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Horizontal Multistage Acid-Fracturing Formulates Development Strategy in Tight Tuba Carbonate Reservoir, North Kuwait

机译:水平多级酸性酸碎屑制剂在北科威特封闭岩石储层中的开发策略

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Tuba is tight carbonate reservoir and one of largest Upcoming Reservoirs in North Kuwait Sabriyah field and subdivided to three main reservoir units (upper, middle and lower). Tuba, though discovered in the 60's, is still relatively under-exploited presently with only ±10 active oil producer wells with very low total production rate compared to other major reservoirs in same field. High reservoir heterogeneity, tightness, and poor fluid properties necessitate the application of fracturing stimulation technology to maximize Conductivity and hence recovery enhancement. Recent technologies in multistage acid Fracturing executed successfully covering multiple layers as first time ever in one of existing two Tuba horizontal wells. The well under study is highly deviated, completed as barefoot in the Upper Tuba reservoir, intersecting multiple sub-layers. Following the positive results of acid fracturing treatments in offset Tuba's vertical wells, the candidate well was selected for first multistage acid fracturing in horizontal wells, to setup the reservoir development plan ensuring high production potential with most cost-effective drilling and completion strategies. Rig-less 5-Stages Acid Fracture treatment was executed in flawless operation. Many technical and operational challenges were faced (Geo-mechanics, stages selection and design, cementing 7in liner) and properly handled within integrated teams with lessons learned are to be considered in next designs and executions. Initial post multistage acid Frack short term production showed productivity improvement by approximately 5 folds of pre-stimulation production. The well showed high decline in production rate within the first one-year production post fracturing stimulation. However, analysis showed that the decline mainly was caused by reservoir depletion rather than fracture conductivity deterioration. The well is under close monitoring for stabilization (rate and pressure). Horizontal PLT is planned to evaluate inflow profile from individual layers to improve next designs. Despite the close results yilded from the multistage acid fracturing in two horizontal wells compared to the results from 7 vertical wells, it is still early to evaluate stimulation potential of horizontal against vertical wells. It needs more production history and more wells to evaluate long term sustainability. Water-flooding is planned to support reservoir development and enhancing stimulation sustainability and by turn recovery factory. First pilot water flooding injector well was commissioned in early 2018, but comprehensive waterflooding analysis is not finalized yet.The initial positive results of first multistage acid fracturing in Tuba reservoir had key contribution to setup Development strategy for the entire TUBA reservoir to expand drilling horizontal wells and complete it with initial multistage fract (MSF) stimulation to maximize reservoir exposure and enhance reservoior productivity that will contribute significantly to the NK production target. Two more horizontal wells were drilled and completed with MSF in late 2018 with initial encouraging enhanced productivity results during cleaning and lifting but were not put yet on production for more comprehensive analysis. ation to improve initial productivity.
机译:Tuba是紧密碳酸盐储层和北科威特萨布里耶的最大储层之一,并细分为三个主储层单位(上部,中低)。 Tuba虽然在60年代发现,但目前仍然具有±10个活性石油生产商井,与同一领域的其他主要水库相比,总生产率非常低。高储层异质性,紧密性和较差的液体特性需要应用压裂刺激技术来最大化导电性并因此恢复增强。多级酸压裂中的最近技术在现有的两个Tuba水平井中的一个中首次执行成功覆盖多层多层。在研究中良好的研究是高度偏离的,在上部大块储存器中赤脚完成,交叉多个子层。在偏移Tuba的垂直孔中酸压裂处理的阳性结果之后,选择候选井在水平孔中进行第一多级酸压缩,以设置储层开发计划,确保具有最具成本效益的钻井和完井策略的高生产能力。在完美的操作中执行钻头减去5-阶段酸性裂缝处理。面临许多技术和运营挑战(地理 - 力学,阶段选择和设计,削弱7英寸衬班)并在综合团队中正确处理,并在下一个设计和执行中考虑了经验教训。初始后多级酸褶皱短期产量显示生产率提高约5倍的预刺激生产。井中的生产率在折磨后的第一个一年的生产术后的生产率下降得多。然而,分析表明,该下降主要是由储层耗竭而不是断裂电导率劣化引起的。井是在密切监测的稳定(速率和压力)。计划水平PLT评估各个层的流入型材,以改善下一个设计。尽管与来自7个垂直孔的结果相比,从两种水平孔中的多级酸压裂的效果很接近,但它仍然早期评估水平孔的刺激潜力。它需要更多的生产历史和更多井来评估长期可持续性。计划水洪水支持水库开发,增强刺激可持续性,转向恢复工厂。首次试点水洪水喷射器井在2018年初进行委托,但尚未确定综合的水上水解分析。第一个多级酸压裂的初始阳性结果在Tuba Choptoir中对整个Tuba水库的开发策略进行了关键贡献,以扩大钻井水平井并用初始多级换挡(MSF)刺激完成,以最大限度地提高水库暴露,并提高对NK生产目标有贡献的储层生产力。 2018年底,钻探两台横向井并完成MSF,初步鼓励在清洁和提升过程中提高生产率,但未在生产中进行更全面的分析。修改初始生产力。

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