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Giving a Boost to Low Pressure Gas Well by Installing Gas Ejector

机译:通过安装燃气喷射器,良好地提升到低压气体

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To further reduce the back pressure on low-pressure gas wells and increase reserves in a mature gas field, a gas ejector project was evaluated and proposed in 2014. Following on-site tests on several gas wells during 2015 the gas ejector was successfully put into service in 2016. Reservoir simulation estimates that 6.4bcf of incremental reserves will be achieved through gas ejector installation by decreasing inlet pressure to 50 psi from 100 psi. Very low capital costs and insignificant operating costs demonstrate positive economics. Existing facilities and availability of high-pressure gas source contribute to the success of this project. The gas ejector was designed and manufactured in China at far more competitive costs that could be obtained in the international market. The application of gas ejector during the past 2 years to reduce back pressure has helped to improve the economics in a mature gas field. Figure 1 shows the location of YC13-1 field facilities.
机译:为了进一步减少低压气井的背压并在成熟的气田中增加储备,2014年评估了气体喷射器项目。在2015年期间对几种气井进行现场测试,将气体喷射器成功投入 2016年服务。储层模拟估计,通过将入口压力降低到100psi,通过燃气喷射器安装将通过燃气喷射器安装来实现6.4BCF。 非常低的资本成本和微不足道的运营成本展示了积极的经济学。 高压气体源的现有设施和可用性有助于该项目的成功。 燃气喷射器以更具竞争力的成本在中国设计和制造,可以在国际市场上获得。 在过去2年中,燃气喷射器在减少背压期间的应用有助于改善成熟的气田中的经济学。 图1显示了YC13-1现场设施的位置。

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