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How to Avoid Bottom Hole Assembly Twist Off Challenges in Underreaming While Drilling Operations Using 4D Finite Element Analysis Modelling

机译:如何避免底部孔组件在使用4D有限元分析建模的钻井操作时扭曲突出次突出的挑战

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Historically underreaming while drilling (UWD) operations were implemented in offshore field in Azerbaijan to decrease Equivalent Circulating Density (ECD) and have better hole quality for casing running. Lithology in this UWD, 8.5 × 10.25-inch section consists of sand and shales with 3-5kpsi Unconfined Compressive Strength (UCS). Well trajectory has planned dogleg severity up to 3-3.5 deg/30m. In such a condition underreaming operations are known to be more challenging and complex compared to conventional drilling with bit only. In the offset well, an operator had fatigue related twist off at the reamer's lower sub connection which contributed to 58 hours of NPT. Our challenge was to come up with the root cause of the twist off and then suggest changes in BHA to avoid this and prove that the modified BHA performs as expected. Our finite element analysis (FEA) based 4D modeling software can identify different vibrations (axial, lateral, stick slip), bending stresses and bending moment of each component in the BHA. Using this software, we were able to come up with the root cause of the twist off, which was due to high bending stress. In UWD there are two cutting structures in the BHA, so optimizing both cutting structures has a significant impact on the overall performance. Successful run key points are to analyze the underreamer placement in BHA, operating parameters selection for different scenarios (when both bit and undereamer are in the same rocks or when the bit is in soft and undereamer is in hard rock), lateral vibrations and whirling phenomenon which can potentially damage and develop fatigue on BHA components. Multiple BHA's were simulated and based on the results the most stable BHA was recommended for the upcoming well. The operator implemented the recommended BHA and a total of 1200m was successfully drilled and opened in one run without any NPT. All directional requirements were achieved and both bit and underreamer came out in good condition which confirmed that the new optimized BHA was stable in the downhole drilling conditions. The liner was also run without any issue confirming the borehole quality. This paper will review the results of analysis and how modeling prediction was validated in the field.
机译:历史上遭到钻井(UWD)操作在阿塞拜疆的海上领域实施,以减少等效的循环密度(ECD),并具有更好的套管运行孔质量。在这个UWD中的岩性,8.5×10.25英寸部分由带有3-5kpsi不包含3-5kpsi的砂砾,具有3-5kpsi的抗压强度(UCS)。井轨迹计划的狗屎严重程度高达3-3.5°/ 30米。在这种情况下,与常规钻井相比,已知劣地操作是更具挑战性和复杂的。在偏移井中,操作员在铰刀的下部连接处具有疲劳相关的扭曲,这导致了58小时的NPT。我们的挑战是提出了扭曲的根本原因,然后建议BHA的变化来避免这种情况,并证明修改的BHA按预期执行。我们的有限元分析(FEA)的4D建模软件可以识别BHA中每个组分的不同振动(轴向,横向,粘滑),弯曲应力和弯矩。使用此软件,我们能够提出扭曲的根本原因,这是由于高弯曲应力。在UWD中,BHA中有两个切割结构,因此优化两种切割结构对整体性能产生重大影响。成功的运行关键点是分析BHA中的次衰减器放置,对不同场景的操作参数选择(当两位和钻头时都在同一岩石中或当该位柔软而且充满激烈的摇滚岩)时,横向振动和旋转现象这可能会损坏并在BHA组件上造成疲劳。模拟了多个BHA的结果,结果建议最稳定的BHA用于即将到来的良好。运营商实施了推荐的BHA,总共1200米被成功钻探并在没有任何NPT的情况下一次运行。所有定向要求都实现了所有定向要求,钻头和底部陷入困境都处于良好状态,证实新的优化BHA在井下钻井条件下稳定。衬里也在没有任何问题的情况下运行,证实了钻孔质量。本文将审查分析结果以及如何在该领域验证建模预测。

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