首页> 外文会议>SPE/IATMI Asia Pacific Oil Gas Conference and Exhibition >Applying Epoxy Resin Technology on Remediation for 3.5 in.Casing Leak:Case Study,South Sulige Gas Field
【24h】

Applying Epoxy Resin Technology on Remediation for 3.5 in.Casing Leak:Case Study,South Sulige Gas Field

机译:应用环氧树脂技术对3.5的修复。泄漏:案例研究,南苏丽气田

获取原文

摘要

In the South Sulige gas field,a casing leak was discovered after a velocity string production failure causedwell SNXXX-02 to be killed because of water traveling from the formation into the wellbore through thecasing leak.This high productivity well urgently needed casing leak remediation to restart production.Instead of a conventional casing patch approach to repair casing leakage,an innovative solution using anepoxy resin system was applied to recover wellbore integrity and return the well to production.In addition,the resin system does not create casing diameter reduction or restriction during the next velocity installation.However,operational histories and field performance in terms of the capability to mill resin inside 3 1/2-in.casing were rare.This paper discusses a case study of applying the epoxy resin system,a rigless operationusing fiber-optic coiled tubing (FOCT)to detect a leak,and then squeezing the epoxy resin using coiledtubing (CT)followed by milling-out after its solidification.The remediation's effectiveness was determined and examined using qualified wellbore pressure testing;this is the first successful application of an epoxy resin in the South Sulige gas field.The recovery ofwellbore integrity helped the operator restart production and maintained the wellbore with no ID restrictionfor ease of the following velocity string installation.Most of the wells in the South Sulige gas field are tubingless directional wells with 3 1/2-in.productioncasing.Implementing a velocity string was widely used as a deliquification method during production.A casing patch was the primary solution to repair casing leakage in this area.This integrated service ofdetecting the casing leakage point and applying the epoxy resin presents a new method of well remediationfor the operator.
机译:在南苏里梅气田中,在速度弦生产失败后发现了一种套管泄漏,导致了由于从形成到井筒的水进入井筒而被杀死。这是高生产率,迫切需要肠道泄漏修复才能重新修复制作。在传统的套管贴片方法中修复套管泄漏的方法,应用了使用苯氧基树脂系统的创新解决方案来回收井眼完整性并返回到生产井。此外,树脂系统不会产生套管直径减小或限制下一步速度安装。在3 1/2-In.Casing内的磨削树脂的能力方面,操作历史和现场性能是罕见的。本文讨论了施加环氧树脂系统的案例研究,无条件的纤维 - 光学卷绕管道(FOCT)以检测泄漏,然后使用线圈(CT)挤压环氧树脂,然后在其Soli后铣掉差异。使用合格的井眼压力测试确定和检查修复的有效性;这是南苏里省气田中环氧树脂的第一次成功应用。韦尔韦尔介的完整性恢复有助于运营商重启生产并保持井筒,无需id限制以下速度弦柱安装。南苏里梅气田的井中的大部分井是无线管道定向孔,31/2-In.Production.implementing在生产过程中广泛用作饮水方法。套管贴片是在该区域修复壳体泄漏的主要解决方案。这种壳体泄漏点和施加环氧树脂的整合服务呈现了操作员良好的修复方法。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号