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Secondary System Return to Service Following the Refurbishment Outage at the Point Lepreau Generating Station

机译:次级系统在点乐尔·生成站的翻新中断后返回服务

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During the latter portion of 2012, the Point Lepreau Generating Station (PLGS) was returned to service following a mid-life refurbishment that commenced in 2008. The plant achieved criticality following refurbishment on 2012 July 25 (30 years to the day of first criticality in 1982) and commercial operation re-commenced on 2012 November 24. In addition to the refurbishment activities for the reactor core that entailed the complete replacement of all 380 fuel channels and associated inlet and outlet feeder pipes, significant refurbishment work was undertaken on the secondary side of the plant. The major activities on the secondary side included replacement of the turbine rotors with the intent of achieving an additional 3-5% power output, a complete re-tubing of the titanium condensers and replacement of the tube-sheets, and dismantling and inspection of the reheaters. The extended duration of the refurbishment outage due to issues with installation of the calandria tubes, an inadvertent incident that caused the low-pressure turbine rotors to be dropped into the Bay of Fundy and the discovery of organic contamination on the turbine rotors prior to restart led to a comprehensive plan for secondary system clean-up and restart following the refurbishment outage. The secondary system at PLGS typically operates on AVT chemistry treatment with morpholine and includes a full-flow condensate polishing plant, which was intended to be run continuously during system clean-up and plant restart. During the initial plant run-up, the morpholine chemistry was exchanged with ammonia to improve upon condensate polisher run times. This paper describes the comprehensive plan that was implemented during the return-to-service of the secondary system and presents the results and lessons learned from the clean-up of the system including impacts on FAC, corrosion product transport and condensate polisher performance.
机译:在2012年后一部分期间,在2008年开始的中生翻新之后,点勒佩发电站(PLGS)返回服务。在2012年7月25日翻新后,该工厂在翻新后实现了临界性(第一次关键性30年1982年)和商业运营于2012年11月24日重新开始。除了需要完全更换所有380个燃料通道和相关入口和出口进料管道的反应堆核心的翻新活动外,在二级方面开展了显着的翻新工作植物。二次侧的主要活动包括更换涡轮转子,目的是实现额外的3-5%功率输出,钛冷凝器的完全重新装入,更换管纸,并拆除和检查再热。由于安装Calandria管的安装而导致的翻新中断的延长持续时间,这是导致低压涡轮机转子的无意事件,导致低压涡轮机转子在涡轮机转子上丢弃到诸如涡轮转子上的有机污染物的发现在翻新中断后次要系统清理和重启的全面计划。 PLGS的二级系统通常在通过吗啉的AVT化学处理上操作,包括全流动缩合抛光厂,其在系统清理和工厂重启期间连续运行。在最初的植物延伸期间,通过氨气交换吗啉化学,以改善冷凝水抛光时间。本文介绍了在二级系统的返回服务期间实施的综合计划,并提出了从系统的清理中吸取的结果和经验教训,包括对FAC,腐蚀产品运输和冷凝器抛光性能的影响。

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