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Achieving Economically Successful Deployment of Coiled Tubing at Sea as Downline to Repair a Gas Pipeline

机译:在海上实现卷绕管的经济成功部署为下行,以修复天然气管道

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Offshore pipeline pre-commissioning activities normally involve the use of downline to permit the communication between surface equipment (normally rigged up in a vessel or rig) and the subsea pipeline injection/vent point. Recently, a major operator in Brazil deployed a 1 3/4-in. coiled tubing (CT) string as downline at sea using a methodology to maintain a smooth bend radius to help reduce fatigue issues during operations. Using CT as downline for this operation saved the operator USD millions by eliminating the need to replace a pipeline section. The 40-kilometer (km) pipeline had a blockage composed of pigs, debris, and hydrates. After two failed interventions, the operator decided to install a subsea hot tap on each side of the plug, displace the hydrocarbon, and clean the pipeline to cut the section and replace it with new pipe. The blockage was located 6 km from the center of the pipeline. CT string was deployed to the seabed (1400 m) and was attached using soft sling in a deployed 8-ton clump weight positioned next to the pipeline. A 25-m flying lead hose was used in the bottomhole assembly (BHA) to connect the CT to the pipeline subsea hot tap near the plugged section and compensate vessel movement. After attaching the CT string on the clump weight, the vessel was moved away from this point to deploy 40 m of the CT on the seabed, forming a smooth bend radius. A Nitrogen generator unit (NGU) was used to displace gas in the pipeline to the production unit flare. Cleaning operations were completed using a pig propelled with filtered seawater provided by pumping equipment located on the production unit. The execution plan required that all fluids be recovered onboard the support vessel through the CT attached to the subsea hot tap. Using CT and established best practices, the team was not only able to clean the pipeline section as planned but also eliminate the need to cut and replace the pipeline section. The CT string was kept under water for more than 170 hours, demonstrating its capability to satisfactorily function as downline equipment during this operation.
机译:海上管道预调试活动通常涉及使用下线以允许表面设备(通常在船舶或钻机中装配)之间的通信以及海底流水喷射/通气点。最近,巴西的主要运营商部署了1 3/4英寸。使用方法来保持平滑的弯曲半径的平线管(CT)弦作为海上的下线,以帮助减少操作期间的疲劳问题。使用CT作为此操作的下线通过消除替换管道部分的需要,将运营商USD百万美元保存。 40公里(km)管道由猪,碎片和水合物组成堵塞。经过两次失败的干预后,操作员决定在插头的每一侧安装海底热龙头,取代碳氢化合物,并清洁管道以切割部分并用新的管道替换它。堵塞距离管道中心有6公里。 CT String部署到海底(1400米),并在坐在管道旁边定位的部署的8吨丛重的柔软吊带上安装。在底座组件(BHA)中使用了25米的飞行铅软管,将CT连接到堵塞部分附近的管道海底热龙头,并补偿血管运动。在将CT串上附着在丛生的重量之后,将容器移开此时,以在海底上部署40米CT,形成平滑的弯曲半径。使用氮气发生器单元(NGU)将管道中的气体移位到生产单元耀斑。使用在生产单元上的泵送设备提供过滤海水的猪完成清洁操作。执行计划要求所有流体通过附加到海底热龙头附加的CT在支撑船上恢复。使用CT和建立最佳实践,该团队不仅可以按计划清理管道部分,而且消除了削减和更换管道部分的需要。将CT串保持在水下超过170小时,证明其在此操作期间令人满意地发挥作用的能力。

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