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Delayed-Release Acid System for Remedial Cleanup of Well Perla-7

机译:延迟释放酸系统,用于补救井Perla-7

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The Perla-7 well experienced lost circulation while drilling the naturally fractured carbonate reservoir. To cure the losses, 285 bbl of various lost-circulation materials (LCMs) were pumped. This plugged the 300-micron slotted liner and resulted in an impairment of production. This paper describes a study of the solids retention by a 300-micron slotted liner and the design, testing, and application of a delayed-release acid system to remediate the plugged well and recover productivity. The well was closed while spotting the delayed-release acid treatment; gas was filling the well from the previous well testing. Coiled tubing (CT) was used along with a proven fluidic oscillator technology that enables better control when matching fluid rates to the most desirable frequency and amplitude of the pressure pulses. When the pressure began rising from the last recorded surface pressure, the well was bled off on the surface to maintain a balanced condition. After the treatment, the well was opened and cleaned out using well testing equipment, flaring hydrocarbons, and spent acid. Logistical considerations resulted in the selection of the in-situ acid-release system instead of conventional treatments. The pumped LCMs dissolved successfully, helping to swiftly recover well productivity. The acid-release treatment was split into two stages, with a 30-minute soaking time between the pumping of the two designed engineered pills. A total of 270 bbl of the delayed-release acid were pumped at a 25% volume/volume concentration. No special tanks were necessary for this operation; the acid-release treatment is neutral on surface and is easily handled until required. The well test interpretation was developed based on a pressure buildup period before and after the treatment, The results returned a fairly good reservoir property, with a Kh of approximately 10 000 md-ft with a consistent skin reduction from 14 to four. There was also a corresponding reduction in the drawdown of 120 psia, which was necessary to achieve the same gas rate of 50 million scf/D. The Perla field is the largest offshore gas reservoir discovered to date in Latin America. The Perla-7 well was drilled in the Cardon IV block, located in the shallow water eastern part of the Gulf of Venezuela. The in-situ acid release treatment is now an alternative option through which to support offshore operations where logistics can be challenging, especially when well remediation is required.
机译:Perla-7经历了钻探天然碎裂的碳酸盐储层的同时经历过循环。为了治愈损失,泵送了285个丢失循环材料(LCMS)的BBL。这堵塞了​​300微米的开槽衬里,导致生产损伤。本文介绍了300微米开槽衬里的固体保留以及延迟释放酸系统的设计,测试和应用,以修复堵塞井并回收生产率。在点发现延迟释放酸处理的同时关闭井;气体从之前的孔测试中填充了井。连续管(CT)与经过验证的流体振荡器技术一起使用,当将流体速率与压力脉冲的最期望的频率和幅度匹配时,可以更好地控制。当压力从最后记录的表面压力开始上升时,井在表面上被吹出以保持平衡条件。治疗后,使用良好的测试设备,喇叭形碳氢化合物和废酸打开井和清除。后勤考虑因素导致选择原位酸释放系统而不是常规治疗。泵浦的LCMS成功溶解,有助于迅速恢复良好的生产率。酸释放处理分为两个阶段,在两个设计的工程丸的泵送之间具有30分钟的浸泡时间。将总共​​270bbl的延迟释放酸以25%体积/体积浓度泵送。这种操作不需要特殊的坦克;酸释放处理是中性的,易于处理直至需要。井测试解释是基于治疗前后的压力累积期,结果返回了一个相当好的储层性能,其中kH约为10 000平方英尺,皮肤持续14至4。 120 psia的缩减还有相应的减少,这是达到相同的5000万SCF / D的燃气速率所必需的。 Perla领域是在拉丁美洲迄今为止发现的最大海上煤气藏。 Perla-7井是在Cardon IV块中钻井,位于委内瑞拉湾的浅水区。现场酸性释放治疗现在是一种替代选择,可以支持海上业务,其中物流可能具有挑战性,特别是在需要良好的修复时。

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