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Influence of Downhole Fluid Behavior Changes on Slickline Operations inBurgan and Magwa Oil Fields, Kuwait

机译:井下液体行为变化对光滑运营寄生和马马油田的影响

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Slickline down-hole flow control devices are always subjected to forces created by differential pressure wherethey are setting in tubing.The standard practice for retrieving a flow control device (e.g. Plug from landing nipple) is to equalize pressuresprior any retrieving attempt.Slickline operators are always focusing on a mechanical surface wire manipulation of down-hole tools and surfacepressure gauge to monitor equalizing pressure, while they overlook the effect of influential down-hole conditionssuch as: fluid level, fluid gradient, gas segregation and phase changes which based on we can calculate anddetermine the actual equalizing pressure.In some cases, the equalizing pressure could not be completed properly due to reservoir fluid behavior changewhile operating or sometimes equalizing ports might be plugged, therefore any retrieving attempt can lead to anunknown events such as:Slickline tool string blown up due to differential pressure during retrieving plug from a landing nipple.Slickline tool string blown up due to huge differential pressure created by asphaltenes bridge plugformation in the tubing.Slickline toolstring blown up during a flowing gradient survey with a portable well test due to chokechanges.Slickline plug stuck in landing nipple, due to the hydrostatic pressure head acting on the plug.Collection of a non representative single phase bottom-hole sample due to downhole phase change.This paper will discuss the newly developed procedures (best practices) resulting from a meticulous study ofdownhole fluid behavior changes and their influence on slickline operations. These best practices allow slickline toreduce this risk to a controlled level and provide a high service performance at low cost. Case histories fromBurgan & Magwa oilfields will be used to illustrate overlooked slickline job failure root causes and how bestpractices contribute in providing innovative low cost service options.
机译:Slickline Down-Hole流量控制装置始终经过差压产生的力,后者在管道中设置。用于检索流量控制装置的标准做法(例如从降落乳头插头)是均衡任何检索尝试的压力机.Slickline运算符总是专注于井下工具和表面压力表的机械表面线操作,以监测均衡压力,而它们忽略了影响的井下孔条件的效果:流体水平,流体梯度,气体隔离和相位变化,基于我们可以计算anddetermine实际均衡pressure.In某些情况下,均衡压力无法完成妥因储层流体行为changewhile操作或有时平衡端口可能被堵塞,因此任何检索尝试可能导致anunknown事件,如:钢丝工具串炸了由于在从着陆Nippl检索插头时差压E.Slickline工具串由于在管道中的沥青桥桥接插件创造的巨大差压而爆炸。在流动的梯度调查期间,由于chokechanges.slickline塞子被堵塞在着陆乳头上,由于静水,因此作用在塞子上的压力头。由于井下相变由于井下相变,非代表性单相底部孔样品的校集。本文将讨论新开发的程序(最佳实践),由Downhole流体行为变化的细微研究和它们对光滑的影响操作。这些最佳实践允许Slickline将此风险归因于受控水平,并以低成本提供高服务性能。杂志历史博览会博物公司和Magwa油田将用于说明被忽视的SLICKLINE作业失败根本原因以及如何在提供创新的低成本服务选项方面做出有助的。

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