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AN INTERESTING APPROACH TO YIELD IMPROVEMENT

机译:一种有趣的屈服改善方法

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Whilst many forward thinking companies invest time, effort and cost into up front work to fix snags which would lead to issues with yield during production, this paper shows the efforts of a company who take things further. With increasing pressure on cost reduction within our industry, companies are looking ever more closely at their manufacturing process. In order to remain globally competitive and even to succeed in their local market every dollar saved here helps the bottom line. However, in many areas there is a danger that lower price equals lower quality and therefore actually higher costs in the end. The approach here involves spending a little more money than normal at the start of project but less than hundreds of dollars and the results show savings of many times more than this outlay. However, it is acknowledged that this does take a little more time to get the job onto the shop floor. The key to this methodology is that it needs the time and effort of a skilled team and time on a production line before the job is started. But as the paper shows it really does improve yield, reduce cost, save the potential issues around repair and gives better reliability. In essence the results of the printing process are analysed, after the components are placed, using X-ray and these results compared to the results after reflow soldering. The resultant pre reflow solder paste shapes are impossible to see with the naked eye or by lifting the components, as the paste would not release evenly. This allows the engineer to determine how differences in printed paste shape and volume react when components are placed on them and how ultimately this affects product quality. Post reflow problems including mid chip solder balls were found to be common faults, as were issues under BGA's including insufficient solder and shorts. The product is run on a "real line" and the results evaluated. Improvements are then made to the stencil design and other key process parameters to ensure that when in production the board is producing acceptable yields.
机译:虽然许多前瞻性思维公司投资时间,努力和成本,以修复障碍,这篇论文显示了一家进一步采取东西的公司的努力。随着我们行业内的成本减少压力,公司正在仔细观察其制造过程。为了保持全球竞争力,甚至在当地市场中成功,每美元保存在这里有助于底线。然而,在许多领域,较低的价格等于质量较低,因此最终成本更高。此处的方法涉及在项目开始时花费比正常的金钱,但不到数百美元,结果显示超过这一费用的数量。但是,承认这确实需要更多的时间来将工作放到车间。该方法的关键是它需要在工作开始之前熟练的团队和时间在生产线上的时间和精力。但随着纸张显示它确实确实提高了收益率,降低成本,保存修复周围的潜在问题并提供更好的可靠性。实质上,分析了打印过程的结果,在放置组分后,使用X射线和这些结果与回流焊接后的结果相比。所得预回流焊膏膏形状是不可能用肉眼或抬起部件的情况下,因为糊状物不会均匀地释放。这允许工程师确定当组件放置在它们上时印刷糊状形状和体积的差异是如何影响它们的最终影响。发现包括中间芯片焊球的后回流问题是常见的故障,就像BGA的问题一样,包括焊料和短裤不足。该产品在“实线”上运行并评估结果。然后对模板设计和其他关键工艺参数进行改进,以确保在生产中,电路板正在产生可接受的产量。

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