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Angostura Phase 3-Rejuvenating Complex Turbidite Fields in OffshoreTrinidad Through a Successful Subsea Tieback Project

机译:AngostuRa第3期通过成功的海底连接项目在离岸替换尼亚的复杂浊度场

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This case study describes the successful outcomes and learnings from a brownfield tie-back project inoffshore Trinidad.The greater Angostura Asset consists of multiple Oligocene-age turbidite sandstonereservoirs with complex geology and compartmentalization.The Asset has produced oil since 2005 fromthin oil rims overlaid by large gas caps.This has been supported by significant gas reinjection andconstrained by gas coning.Commencement of gas sales added value but also increased gas cap blowdown inthe oilfields.The Angostura Phase 3 project was conceptualized to enable gas production from an adjacentgas discovery and extend the overall productive life of the existing oil fields.Key subsurface uncertainties and operational constraints were identified early in the project.Historically,drilling in the Angostura field has been challenging due to the complex geology and compartmentalization.Poor seismic data in the Phase 3 area added complexity to optimal well placement.Ensuring highdeliverability was another critical project requirement.The main reservoir management challenge in theexisting fields was optimizing both oil and gas sales while managing voidage and coning.Limited topsidefacilities and space constrained addition of new gas at flowing at higher pressures.To address these challenges,a multi-disciplinary project team was formed to plan and execute the project.Material balance,detailed geological modeling and numerical simulation were used to understand the impactof key uncertainties on recovery.The integrated evaluation resulted in an optimized development plan withthree subsea gas wells tied back to existing facilities.Production performance of existing wells helpedhighlight critical performance drivers for Phase 3 wells.Modified completion designs along with a flowback and stimulation program during completion helped to maximize productivity.Phase 3 wells have performed at the high levels expected during project design and sanction.Detailedsurveillance(including pressure transient analysis(PTA)and interference testing during completion,start-up and production phases)has continuously helped to optimize production.Oil production in the existingfields has also been improved by better balancing gas sales and injection.The project added significantvalue from the increased gas sales and oil production.This paper discusses the planning,successful execution and impact on the overall value of the AngosturaAsset from the Phase 3 project.Optimized completions along with an improved approach for evaluating stimulation options during completion(detailed near well-bore modelling,real-time PTA and simulation)enabled strong well performance.We highlight some of the critical factors for achieving success inbrownfield tie-back projects including having(right from project inception): multi-disciplinary projectteams,tight coordination with existing operations and a focus on key uncertainties and constraints.Buildingoptionality and flexibility into development plans and being prepared for contingencies have been the othercritical learnings from this project.
机译:本案例研究描述了棕色野生卫卫生间的成功成果和学习,无论是古代山脉三迪达。较大的血管抑制资产包括复杂地质和舱室化的多个少茂域浊度SandstervoIr。自2005年以来,该资产从覆盖的油轮辋覆盖物中产生的油。气囊已经得到了大量气体再注的支持,通过气体销售增加了燃气销售增加了价值,而且还增加了瓦斯帽排污Inthe油田。昂贵的阶段3项目被概念化,使得邻居的燃气生产能够发现并延长整体展开现有油田的生产寿命。在项目早期确定了地下的不确定因素和运作约束。由于复杂地质和分区化,钻探在昂古斯图拉领域的钻井一直挑战。阶段3区域中的地震数据增加了复杂性最佳井放置。腐殖质Itity是另一个关键的项目要求。在管理失控和联系的同时优化石油和天然气销售的主要水库管理挑战。限制了替代渡费和空间在流动时流动的新气体的增加。以解决这些挑战,多-DICISINARINARINAL项目组成计划并执行项目。使用详细的地质建模和数值模拟来了解关键不确定性对恢复的影响。综合评价导致了由返回的海底气井的优化开发计划。设施。现有井的生产性能有助于为第3阶段井的关键性能驱动程序。在完成期间有助于最大化生产率的流量和刺激计划以及在项目设计和制裁期间的高级别进行了最大化和刺激计划.Detailedsurveillance在预期的高级执行(包括G压力瞬态分析(PTA)和完成期间的干扰测试,启动和生产阶段)连续有助于优化生产。通过更好的平衡天然气销售和注射,现有领域的生产也得到了改善。该项目增加了高价汽油销售和石油生产增加。本文讨论了从第3阶段项目的规划,成功执行和对昂密阵容的总体价值的影响。优化完成以及在完成期间评估刺激选择的改进方法(详细介绍了良好的钻孔建模,实时PTA和仿真)启用了强大的性能。我们强调了实现成功的一些关键因素,包括拥有(右从项目成立):多学科项目,与现有运营紧密协调和焦点关于关键的不确定性和约束。制定的开放性和开发的灵活性LAN和为突发事件做好准备是来自该项目的其他批判性学习。

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