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Mitigating Vibration with Roller Reamer Technology Improves Drilling Efficiency in Hard/Abrasive Formation,Sao Francisco Basin,Brazil

机译:带辊铰刀技术的缓解振动提高了钻井磨削效率,巴西圣弗朗西斯科盆地

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When drilling operations commenced in Sao Francisco basin,the operator knew the exploratory well campaign would present a major investment.However,as operations progressed the well costs and time exceeded assessments mainly drilling the 8?production hole section through two hard and abrasive formations.Due to the unconventional nature of the reservoir,well costs must be held to a minimum in the exploration phase to ensure each project is economically viable.To accomplish the objective,several tool technologies were analyzed and proposed with the aim of reducing down-time and tool failures.One of the main issues identified was the high level of shock and vibration(S&V)observed while drilling the Macaubas and Paranoa formations.The environment had a negative impact on drilling efficiency and contributed to tool failures and excessive wear on BHA components leading to additional trips and preventing the operator from achieving higher ROP and run lengths. After an engineering analysis,the drilling team determined the root cause was BHA/bit whirl while along with several other contributing factors related to the challenging hard and abrasive formations. Based on this information,the provider recommended using a roller reamer in the bottom hole assembly (BHA),to mitigate shock and vibration and improve drilling efficiency.Results were positive and the roller reamer reduced NPT and overall well costs in this economically sensitive play.Roller reamers are currently part of standard packed BHA and are being used as a reference for operators experiencing the same type drilling dysfunctions.
机译:当钻井业务在圣兰西科盆地开始时,运营商知道探索性井展会出现重大投资。然而,随着运营进展的井成本和时间超过了主要钻出了8?生产孔部分通过两种艰苦和磨料的地层。对于水库的非传统性质,必须在勘探阶段保持最低成本,以确保每个项目在经济上是可行的。实现目标,分析了几种工具技术,并提出了减少停机时间和工具的目的识别的主要问题的失败是钻头钻猕猴和帕拉诺结构时观察到的高水平的冲击和振动(S&v)。环境对钻井效率产生负面影响,并导致刀具故障和导致BHA部件的过度磨损额外的旅行并防止操作员实现更高的ROP和运行长度。在工程分析之后,钻井团队确定了根本原因是BHA /位旋转,虽然与挑战性艰难和磨料形成有关的其他几个贡献因素。基于此信息,提供者推荐使用辊梁在底部孔组件(BHA)中的钻孔器,以减轻冲击和振动,提高钻井效率。结果是正的,并且在这种经济敏感的比赛中,滚子铰刀降低了NPT和整体井成本。滚轮铰刀目前是标准包装BHA的一部分,并被用作经历相同型钻孔功能障碍的操作员的参考。

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