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Too Much Excitement under Highway 87

机译:在87号高速公路下有太多兴奋

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In early 2005, Santa Clara Valley Water District (District) staff discovered low pressure (~5 psi, or 35 kPa) groundwater leaking into a RCCP section of 66" (168 cm) high pressure pipeline under a major freeway embankment in downtown San Jose. The leak was discovered during an internal eddy current inspection on adjacent PCCP sections of the pipe. Although it had not been detected externally or deemed obvious from modest changes in system flows, leakage from the pipeline during normal operation was a big concern as the pipe operates at 177 psi (1220 kPa). If the leak worsened, it could have undermined the Highway 87 freeway embankment and impacted use of the freeway, caused a major outage in the District water supply system, and posed a major threat to public safety. Investigation showed that the leak occurred in an area under a surcharge embankment, at a joint located between a horizontal and vertical thrust block, where consolidation had been expected and factored into the design. The situation was complicated by construction changes which impacted joint performance; these changes were not adequately recorded on the as-built drawings. Localized deflection/rotation exceeded the design tolerances, leading to a leak at a gasketed joint. External geotechnical investigations showed modest void-space below but not next to the pipeline in this area; it's not clear if these voids were caused solely by consolidation and local pipe movement or by the leakage from the pipe, or a combination of factors. Settlement records strongly suggested that primary settlement due to embankment construction had stabilized. With a basic understanding of the mechanism involved in this failure, staff was able to confidently complete the repairs and put the pipe back into service. Repairs included: installation of flexible Weko-Seals at the two joints of concern; welding of patches on the holes drilled in the 66" (168 cm) pipe to investigate the voids; grouting of the voids below the pipe; patching of cement-mortar lining; and installation of a new precast vault for improved access. This experience produced a number of major "lessons learned" which will help District staff and others in the future.
机译:2005年初,圣克拉拉谷水区(区)员工发现低压(〜5psi,或35千米KPA)地下水进入66“(168厘米)高压管道的RCCP部分,在圣何塞市中心的主要高速公路堤防下。在管道的相邻PCCP部分的内涡流检查期间发现了泄漏。虽然从系统流动的适度变化,从外部检测到外部或视为明显,但在正常操作期间从管道泄漏是一个大问题在177 psi(1220 kPa)运行。如果泄漏恶化,它可能会破坏87公路的高速公路路堤并受到高速公路的影响,导致了在地区供水系统中的重大中断,并对公共安全构成了重大威胁。研究表明,在附加座的区域下发生泄漏,位于水平和垂直推力块之间的关节,预期并考虑到设计中的整合。通过施工变动影响联合绩效的施工变动,情况变得复杂;这些变化未在竣工附图上记录。局部偏转/旋转超过了设计公差,导致垫圈接头处的泄漏。外部岩土性调查显示下面的适度空隙空间,但在该地区的管道旁边;尚不清楚这些空隙仅通过整合和局部管道运动或管道泄漏,或因素的组合而引起。坚决记录强烈建议由于路堤建设引起的主要沉降已经稳定。通过对涉及这项失败的机制的基本了解,工作人员能够自信地完成维修并将管道放回服务。包括维修:在两个关注的关节中安装灵活的Weko-Seals;焊接在66“(168厘米)管道中钻孔的孔上,以研究空隙;管道下方的空隙灌浆;水泥砂浆衬里的修补;以及安装新的预制金库,以改进访问。这种经验一些主要的“经验教训”,将来会帮助地区的工作人员和其他人。

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