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Application of a Light Rig in Deep Exploration Drilling Operations in Nigeria

机译:轻型钻机在尼日利亚深度勘探钻探运营中的应用

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The upsurge in drilling activities in 2004, occasioned by the strong oil prices resulted in a challenging rig market situation such that operators have to plan well in advance to be able to get a rig for the next well campaign. For desperate operators, the only option is innovation or new technology and unusual risk taking. An operator in Nigeria recently adapted a light work over rig of 800 horsepower and 320,000lbs pulling capacity to drill an exploration to 11,000 ft. This was operating the rig at beyond its capacity. Minor modifications were made to the rig to enable the running of casing strings, and operations monitored with the help of wells software, resulting in the successful drilling and abandonment of the A-1x well. The result was a 30% savings of the budget well cost contributed mainly from the slimmer design and lower rig rates of the light 800 hp rig. It is also noted that the light rig was moved in 8 days compared to 23 days planned with the heavier rig. The paper highlights the detailed planning and execution of the drilling phase of the A-1x well and how the capacity issues were addressed leading to the estimated savings of $2million.
机译:在钻探活动的高潮在2004年,受强劲的石油价格引起的,导致在充满挑战的钻机市场形势,使得运营商不得不计划提前做好能够得到下一个好活动钻机。对于运营商绝望,唯一的选择就是创新或新技术和不同寻常的冒险。在尼日利亚运营商近期调整超过800马力钻机和320,000lbs拉动能力钻勘探至11000英尺轻松的工作,这是在操作钻机超出其能力。轻微修改对钻机制造,使套管柱的运行和操作与井软件的帮助下监控,导致A-1X的成功钻探和遗弃很好。其结果是预算以及成本节约30%的主要贡献来自轻薄设计和光800马力钻机的下部钻机率。它也指出,光钻机是8天内转换比例为23天,较重的装备计划。本文着重介绍了详细的规划和A-1X的钻井阶段的执行以及如何容量问题得到解决导致的200万$的估计节省。

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