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Case Study: Drillstring Failure Analysis and New Deep-Well Guidelines Lead to Success

机译:案例研究:钻石故障分析和新的深井指南导致成功

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Three drillstring fatigue failures occurred while drilling two deep wells below 16,500 ft true-vertical depth (TVD) in the U.S.A. midcontinent region. All the failures occurred across 2°/100 ft to 3°/100 ft dogleg severity intervals from 6,000 ft to 8,000 ft. The well conditions (i.e., pipe condition and directional plan) were not significantly different from other deep wells in the area, which had not failed. A deep-well drillstring failure study was conducted which included a review of drillstring inspection reports, daily drilling reports, digital data, technical literature, and engineering analysis for the two wells.
机译:在U.S.A.中间地区的区域钻出两大井中的三个深井(TVD)的深度钻孔后,发生了三个钻孔疲劳失败。所有故障发生在2°/ 100英尺到3°/ 100英尺的嘟嘟声中,从6,000英尺到8,000英尺的严重程度间隔。井条件(即管道状况和方向计划)与该地区的其他深井没有显着差异,这没有失败。进行了深井钻井失败研究,其中包括对两家井的钻头检查报告,日常钻头报告,数字数据,技术文献以及工程分析进行审查。

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