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A New Solution to an Old Problem: Tractored CT Conveyed Real-Time Water Injection Profiling in Ultra Deep Wells

机译:一个旧问题的新解决方案:拖拉机CT在超深井中输送了实时注水曲线

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Intervention work is often necessary in field developments with deep wells to enhance well performance through acid stimulation. Acquisition of flow profile data in these wells is also vital for decision making. Deploying rigless solutions for monitoring of well enhancements and injection zones in the extended reach wells presents both technical and economic challenges given the tortuous nature of these wells, dogleg severity, considerable variations in azimuth and hole inclination, washouts and general hole conditions. Significant intervention cost savings have been observed since hydraulic tractor-aided coiled tubing (CT) intervention was introduced in ultra deep wells in the development of a Saudi Arabian field three years ago. Specific stimulation benefits include reduction to skin damage, improved drawdown, and treatment gains from injectivity increase. While tractor aided coiled tubing has largely been demonstrated as a preferred deployment technique for cost-effective acid stimulation and memory production logging in extended reach wells, the subjects of real-time evaluation of treatment effectiveness and injection zone monitoring have remained an industry challenge. The limitations of memory production logging have been compounded by spinner failure from organic residue dropouts in the wellbore while logging (which cannot be identified with the memory production logging tools until the end of the job). Apart from the lost time and loss of data, operational cost is extended beyond the allocated budget from re-runs, thereby adversely affecting development schedules. From this experience evolved a design to run real-time production logs in such challenging wells with potential for triggering data problems and delivering better quality wells. With improvements in job design, the first real-time production logging job trial was successfully performed in a 9.1 km well with a measured depth to the true vertical depth (MD/TVD) ratio greater than 3.44 in Saudi Arabia. This case study reveals how real-time information was employed to effectively stimulate and perform real-time production logs of an ultra deep well in Saudi Arabia. Practically, the work shows that effective stimulation and real-time production logging are possible in ultra deep wells.
机译:干预工作通常是在野外井的现场发展中,以通过酸刺激提高良好的性能。在这些井中获取流动简介数据对于决策也至关重要。为监测扩展到达井的井增强和注射区域的部署Rigless解决方案呈现出技术和经济挑战,鉴于这些井的曲折性质,Dogleg严重程度,方位角和空穴倾斜,冲洗和通用孔条件的曲折性质。自三年前在沙特阿拉伯领域开发的超深井中引入了液压拖拉机辅助盘绕管(CT)干预,因此观察到显着的干预费用节省了。具体的刺激益处包括降低皮肤损伤,改善缩减和从注射性增加的处理。虽然拖拉机辅助盘管在很大程度上被证明为具有成本效益的酸刺激和记忆生产测井的优选部署技术,但治疗效果和注射区监测的实时评估的受试者仍然是一个行业挑战。记录的局限性通过井眼中的有机残留滴输出的旋转器失败,在记录时(不能用内存生产测井工具识别直到作业结束)。除了丢失的时间和数据损失之外,运营成本超出了重新运行的分配预算之外,从而产生了对发展计划的不利影响。从这个经验中断了一种设计,可以在这种具有挑战性的井中运行实时生产日志,具有触发数据问题并提供更好的质量井。随着工作设计的改进,第一个实时生产记录作业试验在9.1km良好的情况下成功进行,测量深度到真正的垂直深度(MD / TVD)比例大于3.44在沙特阿拉伯。本案例研究揭示了利用实时信息如何有效刺激和执行在沙特阿拉伯的超深井的实时生产日志。实际上,工作表明,在超深井中可以实现有效的刺激和实时生产测井。

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