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A Recent Gulf of Mexico Cavity Completion

机译:最近墨西哥湾的洞穴完成

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摘要

Production was dramatically improved by cavitating (intentionally producing sand) an offshore gas well on the Gulf of Mexico Shelf. The cavity completion was conducted over a period of 10 days and involved producing the well through temporary equipment in order to safely produce, collect, and dispose of the produced sand. No hydrocarbon emissions resulted since production could be routed back through the permanent facilities. Following the operations, the well was returned to flow through the permanent facilities at a much higher producing rate, with much lower sand production. Prior to the cavity completion operations, the well had been choked back to a low gas rate, <1 MMscfd, due to sand production. The low gas rate was insufficient to continuously lift liquids, causing the well to become liquid loaded and/ or slug. The well was evaluated for a sand control completion, but this type of repair was felt to entail too much economic risk due to significant reservoir unknowns. Further evaluation suggested that the well had the attributes for a successful cavity completion. This paper will discuss the cavity completion evaluation process employed and operational results and learnings. A similar process may be applicable to other wells.
机译:通过在墨西哥湾的海湾上储蓄(有意地生产沙子),通过在墨西哥湾的海外储蓄井中显着改善了生产。腔状完成在10天的时间内进行,并且涉及通过临时设备生产井,以安全地生产,收集和处理产生的砂。由于生产可以通过永久性设施进行生产,因此不会产生碳氢化合物排放。在运营之后,井被恢复流经永久性设施,以更高的生产率,砂生产较低。在腔腔完成操作之前,由于砂生产,井被窒息回气速,<1 mmscfd。低气体速率不足以连续提升液体,使得井成为载荷和/或块的液体。井是评估了一个防抱道完成,但由于重要的水库未知,感觉这种类型的修复被认为是由于过多的经济风险。进一步的评估表明,井有一个成功的腔成功完成的属性。本文将讨论采用和运营结果和学习的腔完成评估过程。类似的过程可能适用于其他井。

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