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ANALYSIS OF STEAM TURBINE INSTABILITIES OF A100 MW COMBINED CYCLE POWER PLANT

机译:A100 MW联合循环发电厂汽轮机稳定性分析

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An analysis of the vibration field of the steam turbine in a combined cycle power plant has been used to identify the causes of the plant rejection at commissioning. The steam turbine group consists of a high pressure turbine connected through a gear box to a medium and low pressure turbine. The high vibration level in the main steam turbine journal bearings caused the plant can't reach nominal power 100 MW, and at approximately 43 MW the plant was rejected.Vibration is measured through proximity non-contact sensors (two per bearing at 90°), which give relative displacements between shafts and the bearing housing. Accelerometers are also located in the bearing housing.
机译:组合循环发电厂中汽轮机振动场的分析已被用来识别植物排斥在调试的原因。蒸汽轮机组包括通过齿轮箱连接到介质和低压涡轮机的高压涡轮机。主蒸汽涡轮轴承的高振动水平导致植物无法达到标称功率100mW,并且在植物被拒绝约43兆瓦。通过接近的非接触式传感器(每轴两个轴承为90°的两个轴承)测量振动。 ,这给出了轴和轴承壳之间的相对位移。加速度计也位于轴承壳体中。

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