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Salt Water Disposal System Modification during Low Water Flow Rates from Khurais Fields

机译:盐水处理系统改性在克什内斯田的低水流率期间

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The Khurais Central Processing Facility (KhCPF) includes four salt water disposal (SWD) systems distributed among four oil trains. Each SWD system is comprised of one water-oil separator (WOSEP), three 33% salt water disposal pumps, and necessary piping from pump discharge, which are terminated at the water injection header. The SWD system has been designed to accommodate ultimate produced formation water (30% water cut from Khurais fields); however, due to the unexpected very low water flow rate from the fields since the commissioning period of the facility, SWD systems are encountering inconvenient operation and frequent equipment failure. To eliminate the operational difficulties and protect the major pieces of equipment, various options were evaluated. The most optimum solution found was to divert salt water from three WOSEPs to a depressurizing vessel by pressure transfer and then recycling it back to a single train. The benefits from modification included — energy conservation by minimizing the running of salt water disposal pumps, reducing the environmental impact and huge operational flexibility for the facility — even if the water cut increases in the future. This modification is expected to be one of the best solutions for the gas-oil separation plants (GOSPs) that that are facing operational difficulties due to low water flow rates from an oil field. This paper describes the modifications in a salt water disposal system, hydraulic assessments, HAZOP study and the field modification that are planned in the KhCPF for the recycling of salt water from the WOSEP to the depressurizing vessel.
机译:Khurais中央加工设施(KHCPF)包括分布在四次油列中的四种盐水处理(SWD)系统。每个SWD系统由一个水 - 油分离器(WOSEP),三个33%的盐水处理泵,以及来自泵放电的必需管道,这些管道在注水头上终止。 SWD系统旨在适应最终产生的地层水(30%从Khurais领域切割);然而,由于设施的调试时间以来场外出现意外的极低水流量,SWD系统遇到了不方便的操作和频繁的设备故障。为消除操作困难并保护主要设备,评估各种选择。发现最佳的溶液是通过压力转移将盐水从三个WOSEP转移到减压血管,然后将其回收回到一列火车。修改的益处包括 - 通过最大限度地减少盐水处理泵的运行,降低设施的环境影响和巨大操作灵活性 - 即使未来的污水也会增加,降低节能。该修改预计将成为气体油分离植物(GOSP)的最佳解决方案之一,这是由于来自油田的低水流率而面临的操作困难。本文介绍了盐水处理系统,水力评估,HAZOP研究和KHCPF中计划回收从WOSEP到减压容器的盐水的改进。

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