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Improving the Weld Procedures for Repairing Aged Heat Resistant Nickel-Base HP-Mod Alloy Reformer Tubes

机译:改善修复老化耐热镍基HP-MOD合金重整管的焊接程序

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Repair welding of service-exposed, aged Heat Resistant Nickel-Base alloys is notorious for being extremely difficult. There is a high propensity for cracking in the heat affected zone of the weld which manifests during or immediately after the welding process. Industry experience and current literatures converge upon one conjecture-that the success of the weld is based largely on optimistic 'trial and error'.Prior Failure Analysis of characteristic weld cracks observed upon welding revealed the root cause to be the synergistic action of high Heat Input of the welding process and the residual stress which lead to a localized Creep Embrittled HAZ which eventually failed due to brittle intergranular fracture. Three weld parameters were identified for the reduction of heat input and residual stress; Groove design, Welding Pattern and Interpass Temperature. The joint was upgraded from a Double-angle V-groove to a U-groove, use of a Stringer Pattern instead of Weaving and a higher Interpass Temperature.Mechanical testing revealed that the modified procedure was superior. Void Counts of the HAZ showed a reduction in void percentage from 5.31% (Original Procedure) to 0.74% (New Procedure) near the tube's ID and a reduction from 13.3% (Original Procedure) to 3.40% (New Procedure) at OD areas. Comparative Hardness Testing of the Original and New Weld Procedures' weld joints concurred with the creep void analysis. Hardness profiles of the New Procedure showed higher values compared to the Original Procedure suggesting superior tensile strength of and less fissuring.The success of the new weld procedure was further authenticated by tensile testing. The 0.2% Yield Strength of the New Procedure was found to be 383.18N/mm~2 versus 339.70N/mm2 (Original Procedure) reflecting an improvement of 43.48N/mm2. UTS results also reflected an increase from an average of 475.10N/mm~2 (Original Procedure) to a superior 492.55N/mm~2 (New Procedure).
机译:维修焊接服务暴露,老化耐热镍基合金对于极其困难而言是臭名昭着的。在焊接期间或在焊接过程之后的焊缝的热影响区域中裂开具有很高的倾向。行业经验和当前文献会聚在一个猜想之上 - 焊缝的成功主要基于乐观的“试验和误差”。在焊接时观察到的特征焊缝裂缝的衰竭分析表明,根本原因是高热输入的协同作用焊接过程和残余应力导致局部蠕变脆弱的HAZ,其最终由于脆性骨折而失效。鉴定了三个焊接参数,用于减少热输入和残余应力;沟槽设计,焊接图案和层间温度。该接头从双角V形槽升级到U形槽,使用纵梁图案而不是编织,并且更高的接口温度。显示改进的程序优越。 HAZ的空隙计数显示在管道ID附近的5.31%(原始程序)到0.74%(新程序)的无效百分比减少,从OD区域的13.3%(原始程序)减少到3.40%(新程序)。对比较硬度试验的原始和新的焊接程序的焊接关节调节,蠕变无效分析。与建议较高的抗拉强度的原始程序相比,新程序的硬度简档显示出更高的值,表明裂缝的卓越拉伸强度。通过拉伸检测进一步认证新的焊接程序的成功。发现新程序的0.2%屈服强度为383.18N / mm〜2,反映了43.48N / mm2的提高。 UTS结果还反映了平均值的475.10n / mm〜2(原始程序)增加到优越的492.55n / mm〜2(新程序)。

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