首页> 外文会议>International Symposium on Rarefied Gas Dynamics >Solid Rocket Motor Backflow Analysis For CONTOUR Mishap Investigation
【24h】

Solid Rocket Motor Backflow Analysis For CONTOUR Mishap Investigation

机译:固体火箭电机回流分析,用于轮廓ishap调查

获取原文

摘要

A procedure developed for free molecule modeling of plume backflow from a STARTM 30BP solid rocket motor is presented for work performed in support of the Comet Nucleus Tour spacecraft mishap investigation. Good general agreement is established with DSMC flowfield results, with interesting deviations developing as the plume backflow approaches the spacecraft surfaces closely, providing insights regarding characteristics of the surface Knudsen layer. Also, investigation of related free expansion results indicate significant discrepancies exist between the rarefied techniques and the continuum results from which their starting surfaces were created. The nature of these differences suggests that convective fluxes to CONTOUR may have been much higher than the rarefied analyses indicated.
机译:为来自STARTM 30BP固体火箭电动机的Plume回流的自由分子模型开发的程序,用于支撑彗星核心游船飞船监测研究。使用DSMC流场的结果建立了良好的综合协议,随着羽流的回流密切接近航天器表面,具有有趣的偏差,提供关于表面knudsen层的特性的见解。此外,相关无效膨胀结果的调查表明,稀土技术与连续性结果之间存在显着的差异,从而产生了它们的起始表面。这些差异的性质表明,对流助熔剂可能已经远高于所指出的稀污染分析。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号