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Development status of LOX/LCH4 rocket engine

机译:LOX / LCH4火箭发动机的开发现状

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IHI Corporation and IHI Aerospace have been continuing the research and development of LOX/Methane regenerative-cooled rocket engine since 2008. LOX/Methane regeneratively-cooled rocket engine is expected to bring many advantages to reality for future propulsion system, such as high performance, reusability, long storage and so on. The engine adopted Gas Generator Cycle with regeneratively-cooled chamber. In 2011 and 2012, the first hot firing tests of the engine were successfully conducted. In 2013, the engine components have been modified almost close to prototype model, and the engine system hot firing has been conducted. This paper describes the status of the 100kN thrust class LOX/Methane regeneratively-cooled rocket engine and the results of sea level hot firing tests held in 2013.
机译:自2008年以来,IHI Corporation和Ihi Aerospace一直在继续研发Lox /甲烷再生冷却火箭发动机的研发。Lox /甲烷再生冷却火箭发动机预计将为未来推进系统提供许多优势,如高性能,可重用性,长存储等。该发动机采用具有再生冷却室的气体发生器循环。 2011年和2012年,成功进行了发动机的第一个热火试验。 2013年,发动机部件几乎接近原型模型,已经进行了发动机系统热烧制。本文介绍了100KN推力级LOX /甲烷再生冷却火箭发动机的状态以及2013年举行的海平热火试验结果。

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