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SCR Performance Enhancements for NO_X Compliance and Reduced Load Operation

机译:SCR性能增强,以符合NO_X标准并减少负载运行

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The operating envelope for a coal-fired selective catalytic reduction (SCR) system is constrained by the presence of sulfur trioxide (SO_3) in the flue gas. SO_3 produced in the boiler limits the minimum operating temperature of the SCR reactor, which affects the ability to inject ammonia and control NO_X emissions during reduced-load operation. In addition, SO_3 produced in the boiler and by the SCR catalyst itself forces operation with low ammonia slip to avoid air heater fouling. Consequently, SCR reactors must be operated at a higher average reactor potential, which increases catalyst consumption and further elevates SO_3 production. As a result of the Cross-State Air Pollution Rule (CSAPR) and the Ozone National Ambient Air Quality Standard (NAAQS), utilities are faced with the need to achieve further reductions in annual and ozone-season NO_X emissions, which will require reductions in their NO_X emission rates during higher-load operation and the ability to maintain the SCR system in operation during reduced-load operation. SO_3 removal upstream of the air heater, and ideally upstream of the SCR reactor itself, is becoming an increasingly important tool for meeting these challenges. Several examples are provided here illustrating how utilities are evaluating the concept of reducing NO_X emissions by removing SO_3 upstream of the air heater, and then operating their SCR system at slightly elevated levels of ammonia slip. Duke Energy has used their "pre-SCR" SO_3 mitigation systems at the Gibson station to allow ammonia injection during reduced-load operation for over seven years. Duke is performing extensive testing in the summer of 2016 to extend this capability to allow even lower-load operation at Gibson and at other Duke plants. An overview of the testing at Gibson is provided here.
机译:烟气中三氧化硫(SO_3)的存在限制了燃煤选择性催化还原(SCR)系统的运行范围。锅炉中产生的SO_3限制了SCR反应器的最低运行温度,这会影响低负荷运行期间注入氨气和控制NO_X排放的能力。此外,锅炉中产生的SO_3和SCR催化剂本身会以低氨泄漏的方式强制运行,以避免空气加热器结垢。因此,SCR反应器必须在更高的平均反应器电势下运行,这增加了催化剂消耗并进一步提高了SO_3的产量。由于《跨州空气污染规则》(CSAPR)和《臭氧国家环境空气质量标准》(NAAQS),公用事业公司面临着进一步减少年度和臭氧季节NO_X排放量的需求,这将需要减少它们在高负荷运行期间的NO_X排放率,以及在低负荷运行期间保持SCR系统运行的能力。在空气加热器上游,最好是在SCR反应器本身上游,SO_3的去除正成为应对这些挑战的越来越重要的工具。这里提供了几个示例,这些示例说明了公用事业公司如何通过去除空气加热器上游的SO_3,然后在略微升高的氨泄漏水平下运行其SCR系统,来评估减少NO_X排放的概念。杜克能源公司(Duke Energy)在吉布森站使用其“ SCR前” SO_3缓解系统,允许在减轻负荷的操作过程中注入氨已有七年之久。杜克将在2016年夏季进行广泛的测试,以扩展此功能,以允许在Gibson和其他杜克工厂进行更低负荷的运行。此处提供了吉布森测试的概述。

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