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Field measurement and analysis on the prestress loss of a long-span PC box Girder Bridge

机译:大跨度PC箱梁桥预应力损失的实测与分析。

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The crack and large deflection of long-span PC box Girder Bridge is common in their service stage. The lower estimation for the loss of prestress is one of possible reasons. Combined with a long-span prestressed concrete box girder bridges, the loss of longitudinal and vertical prestress of a long-span PC box girder bridge is measured during the construction and service stage. Based on the measured results, the loss of the longitudinal and vertical prestress of the long-span PC box girder bridge is analyzed by GA-ANN method and the code of JTG D62-2004, respectively. The results demonstrate that the instantaneous loss of the longitudinal prestress is more than 40% of the designed value, and the total loss of the vertical prestress is about 40% more than the designed one as well. The value of the prestress loss is much higher than the expected one of the design. The reason lies in the inappropriate construction technology, such as not tension the prestress to the designed value, tension at an early age, and excessive different of the tube wobble and so on. Therefore, the engineering quality control must be strengthened during the construction stage of the long-span PC box girder bridge for avoiding excessive prestress loss.
机译:大跨度PC箱梁桥的裂缝和大挠度在其使用阶段很常见。对预应力损失的较低估计是可能的原因之一。结合大跨度预应力混凝土箱梁桥,在施工和使用阶段对大跨度PC箱梁桥的纵向和竖向预应力损失进行了测量。根据实测结果,分别采用GA-ANN方法和JTG D62-2004规范分析了大跨PC箱梁桥的纵向和竖向预应力损失。结果表明,纵向预应力的瞬时损失大于设计值的40%,垂直预应力的总损失也比设计值大40%左右。预应力损失的值比设计中的预期值高得多。原因在于不适当的施工技术,例如不将预应力张紧至设计值,过早张紧以及管摆的差异太大等。因此,在大跨度PC箱梁桥的施工阶段,必须加强工程质量控制,以免造成过多的预应力损失。

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