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Fuzzy Control of Welding Trolley Speed Based on PLC

机译:基于PLC的焊接小车速度模糊控制

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In the course of modern steel rolling production, laser welding machine positioning system with welding trolley as the core device of is automated, which provides the possibility of continuous and efficient production of steel rolling. The quality of welding seam has been an obstacle of automatic and efficient production. Among them, speed of the welding trolley is an important factor affecting the quality of welding. In this paper, the fuzzy control of the welding trolley is adopted to make the driving of the trolley more stable and reduce the interference caused by the startup and stop of the motor, frictional force change of the ball screw, change of resistance in the walking process and the like. Speed change can be traced and its effect on the welding quality tends to be minimized, enabling the automation of the mill's production to be further improved. Since this project is based on the modification of the old B & R positioning system for the laser welding machine in pickling section of the cold rolling mill, Siemens S7-300 PLC program is used instead of the original B & R positioning system for position control in this project. Fuzzy control of welding trolley speed is applied to Siemens PLC program in order to realize its function and carry out corresponding research in this paper.
机译:在现代钢轧制生产过程中,激光焊接机定位系统具有焊机作为芯装置的自动化,这提供了连续高效地生产钢轧制。焊缝的质量是自动高效生产的障碍。其中,焊机的速度是影响焊接质量的重要因素。在本文中,采用焊机的模糊控制使推车的驱动更稳定,减少由起动和停止电机的干扰,滚珠丝杠的摩擦力变化,抗散际过程等。可以追踪速度变化,并且其对焊接质量的影响趋于最小化,从而实现了磨机的生产的自动化进一步改善。由于该项目基于冷轧机酸洗件的激光焊接机的旧B&R定位系统的修改,因此使用Siemens S7-300 PLC程序代替原始的B&R定位系统,用于定位控制在这个项目中。焊接手推车速度的模糊控制应用于西门子PLC程序,以实现其功能并在本文中进行相应的研究。

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