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Experimental Investigation of Steady-State Applied-Field Magnetoplasmadynamic Thrusters at Institute of Space Systems

机译:航天系统研究所的稳态应用磁场磁等离子体动力推进器的实验研究

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The applied-field magnetoplasmadynamic thruster AF-MPD ZT1 was successfully put in operation at IRS. The thruster operated in steady-state mode with Argon as propellant at low electric arc power of 6 kW. Discharge voltage and power increased as expected almost linear with applied magnetic flux density. The variation of mass flow rate ratio between anode and cathode gas towards higher cathode gas fraction showed increasing thrust and thrust efficiency at applied magnetic flux density of 0.1 T and are comparable with DLR's X13 thruster. Additionally a steady-state 100 kW AF-MPD thruster SX3 was developed, set in operation and preliminary characterized at IRS. The SX3 thruster was operated at relatively low arc powers up to 30 kW and applied magnetic flux density of 0.1 T generated by the modified ZT coil. Due to low arc current and magnetic flux level, the AF-MPD ZT1 thruster achieved thrust of 70 mN and exhaust velocity up to 10 km/s at 6 kW arc power and up to 6 % thrust efficiency. The SX3 thruster reached thrust of 362 mN and thrust efficiency more than 12 % in steady state-operation at 25 kW arc power and at applied magnetic flux density of 0.1 T. However both thrusters have been operated at limited magnetic fluxes only. For SX3 a total operation time of more than 3600 s together with 30 ignitions could be accumulated. The electrodes, however, do not show significant erosion nor a respective degradation. The performances of thrusters provide an outlook for future investigations on AF-MPD thrusters at IRS and give a hint to improvement in thrust efficiency of presented devices with the new applied-field coil, which will be manufactured in the future to produce magnetic flux densities up to 0.6 T allowing further increase in thrust efficiency up to 30 %.
机译:磁场等离子推进器AF-MPD ZT1在IRS成功投入运行。推进器以氩气为推进剂以6 kW的低电弧功率在稳态模式下运行。放电电压和功率按预期增加,几乎与施加的磁通密度成线性关系。阳极气体和阴极气体之间的质量流速比朝着较高的阴极气体分数的变化表明,在施加的磁通密度为0.1 T的情况下,推力和推力效率增加,并且可与DLR的X13推进器相提并论。此外,还开发了稳态100 kW AF-MPD推进器SX3,投入运行并在IRS进行了初步表征。 SX3推进器在高达30 kW的相对较低的电弧功率下运行,并通过改进的ZT线圈产生了0.1 T的施加磁通密度。由于电弧电流和磁通量水平低,AF-MPD ZT1推进器在6 kW电弧功率下的推力达到70 mN,排气速度高达10 km / s,推力效率高达6%。在25 kW电弧功率和0.1 T的施加磁通密度下,SX3推进器在稳态运行中达到362 mN的推力,推力效率超过12%。但是,这两种推进器仅在有限的磁通量下运行。对于SX3,可以累积超过3600 s的总运行时间以及30次点火。然而,电极没有显示出明显的腐蚀或相应的降解。推力器的性能为美国国税局对AF-MPD推力器的未来研究提供了展望,并暗示了采用新型应用磁场线圈的现有设备的推力效率的提高,该器件将在未来制造以提高磁通密度到0.6 T,可以将推力效率进一步提高到30%。

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