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Investigation and experimental simulation of performance deterioration of microwave discharge ion thruster μ10 during space operation

机译:空间运行过程中微波排放离子推进器μ10性能劣化的研究及实验模拟

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摘要

In space operation of the microwave discharge ion thruster mu 10 on the asteroid explorers Hayabusa and Hayabusa2, the propellant utilization efficiency deteriorated much more than in the ground endurance test. In this study, a fault tree analysis and experimental simulations of space operation were performed, focusing on the grid-derived internal carbon contamination. It was found that the performance deterioration due to the wave-guide contamination matched that in Hayabusa2 qualitatively and quantitatively. Based on the experimental verification, the future performance is experimentally predicted.
机译:在小行星探险勘探器Hayabusa和Hayabusa2上的微波排放离子推进器Mu 10的空间运行中,推进剂利用效率远远超过地面耐久性测试。在本研究中,进行了故障树分析和空间操作的实验模拟,专注于网格衍生的内部碳污染。结果发现,由于波浪引导污染引起的性能劣化与Hayabusa2的定性和定量相匹配。基于实验验证,未来的表现是通过实验预测的。

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