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Management strategy and technical plan used to select, qualify and procure a new 20.9' L-1 stage steam turbine bucket

机译:用于选择,资格和采购新的20.9“L-1级汽轮机桶的管理战略和技术计划

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Three (3) 400 MW turbine-generators operated by ATCO Electric share the same 33.5" Last Stage Blade (LSB) and 20.9" L-1 steam turbine bucket designs. In 1994 one of these turbines experienced a number of cracks at the tie-wire hole of the L-1 buckets. These cracks have generally been attributed to corrosion fatigue initiation, followed by high cycle fatigue propagation. Industry experience with the L-1 bucket design indicates this problem has occurred in a significant number of these machines operated for more than ten years. Because of the high potential cost of dealing with the fatigue damage as a maintenance problem, ATCO decided to select a new L-1 design from the several solutiosn offered to the industry. To improve the reliability of the L-1 rows, a new design offered by the original equipment manufacturer (OEM) was selected that eliminated the troublesome tie-wire hole and also offered continuous coupling by means of integral covers. The integral covers also eliminated tenon cracking associated with the original design. The new L-1 design provided a modest improvement to the stage efficiency by eliminating the tie-wire obstruction i nthe flow path while also offering an improved airfoil profile. This paper presents details of the L-1 management strategy and the technical evaluation program that ATCO undertook to qualify the new bucket design. In close cooperation with the OEM, features of the new L-1 were evalauted in terms of stresses, frequencies and fatigue life, then compared against the same information obtained for the original design. As a check, natural frequencies and mode shapes obtained in the analysis were compared with OEm telemetry test data. Aero-elastic dampig was calculated and mechanical damping was derived from telemetry data to ensure blade stability under all operating conditions. At present, the first new row of 20.9" L-1 buckets has operated satisfactorily since 1998.
机译:由Atco Electric操作的三(3)个400 MW涡轮发电机相同的33.5“最后阶段刀片(LSB)和20.9”L-1汽轮机铲斗设计。 1994年,其中一台涡轮机在L-1桶的拉线孔中经历了许多裂缝。这些裂缝通常归因于腐蚀疲劳引发,其次是高循环疲劳繁殖。 L-1铲斗设计的行业经验表明,这一问题发生在20多年以上的这些机器中。由于处理疲劳损坏作为维护问题的高潜力成本,Atco决定从为行业提供的几个Solutiosn选择新的L-1设计。为了提高L-1行的可靠性,选择了由原始设备制造商(OEM)提供的新设计,从而消除了麻烦的扎线孔,并通过整体覆盖提供了连续的耦合。整体覆盖物也消除了与原始设计相关的榫裂。新的L-1设计通过消除连杆障碍I n流动路径,为阶段效率提供了适度的改善,同时还提供改进的翼型型材。本文介绍了L-1管理战略的详细信息和Atco承诺资格新的桶设计的技术评估计划。与OEM密切合作,新L-1的特征在应力,频率和疲劳寿命方面进行了评估,然后与原始设计获得的相同信息进行比较。作为在分析中获得的校验,在分析中获得的自然频率和模式形状与OEM遥测测试数据进行了比较。计算航空弹性Dampig,并从遥测数据中获得机械阻尼,以确保在所有操作条件下的叶片稳定性。目前,自1998年以来,第一个新行为20.9“L-1桶的运作令人满意。

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