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Industrial Study on a New Technology of Reducing SO2 Emission in Sintering Flue Gas

机译:减少烧结烟气中SO2排放新技术的工业研究

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摘要

In this paper,a new approach of reducing SO2 emission in sintering flue gas is proposed.The principle is that some kind of additives is introduced into feed mix,the additives decompose into NH3 in sintering process during heating,the NH3 reacts with SO2 gas to form ammonium sulphate solid particles,the particles are captured as dust by ESP,so the removal of SO2 in sintering flue gas is achieved.The study results show that the concentration of SO2 in sintering flue gas decreases gradually with the increase of additive amount,when the specific quantity of additive is 3.02kg per ton mix,the decreasing rate of SO2 is up to 81.33%(mass).Since sintering dust must be recycled as raw materials,in order to solve the problem of flue gas SO2 concentration is gradually increasing,the approach of increasing the amount of additive can be taken,or the dust is separately treated for sulfur removal before being used as raw sintering material.The new approach of reducing SO2 emission in sintering flue gas has advantages of low investment,small occupation area and low operation cost.Moreover,the additive is inexpensive and readily available,so sintering cost is not increased obviously.
机译:本文提出了一种减少烧结烟气中SO 2排放的新方法。其原理是在进料混合物中引入某种添加剂,在加热过程中,添加剂在烧结过程中分解为NH 3,NH 3与SO 2气体反应生成形成硫酸铵固体颗粒,通过电除尘器将其捕集为粉尘,从而实现了烧结烟气中SO2的去除。研究结果表明,随着添加量的增加,烧结烟气中SO2的浓度逐渐降低。每吨混合料的添加量为3.02kg,SO2的降低率高达81.33%(质量)。由于必须回收烧结粉尘作为原料,以解决烟气中SO2浓度逐渐升高的问题,可以采用增加添加剂量的方法,也可以将粉尘单独用作硫磺烧结原料之前进行脱硫处理。减少烟道中SO 2排放的新方法由于其具有投资少,占地面积小,运行成本低的优点。而且该添加剂价格便宜且容易获得,因此烧结成本没有明显增加。

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