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The structural dynamics analysis of the main injector LOX inlet tee and its redesign

机译:主喷油器LOX进气三通的结构动力学分析及其重新设计

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A ground test of a specially instrumented Space Shuttle Main Engine (SSME) revealed excessively high strains in the high pressure Liquid Oxygen (LOX) inlet line which carries LOX to the Main Injector. The inlet tee acts as a manifold which utilizes two splitter vanes to direct the flow of LOX into the main injector. When the high strains were discovered, it was thought that these splitter vanes, coupled with high energy flow was the source. This resulted not only in high strains in the LOX inlet tee, but excessive vibration at a frequency of 4000 Hz located at the gimbal bearing, and at the main injector. This was later to be known as The 4kHz Phenomenon. The dynamic analysis which was used to predict the response due to the 4kHz phenomenon and the analysis used to aid in the design modification required to the hardware to reduce or eliminate the phenomenon is examined.

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