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Interbed Modeling to Predict Wellbore Damage for Big Hill Strategic Petroleum Reserve

机译:夹层模型预测大山战略石油储备的井筒伤害

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摘要

Oil leaks were found in wellbores of Caverns 105 and 109 at the Big Hill Strategic Petroleum Reserve site. According to the field observations, two instances of casing damage occurred at the depth of the interbed between the caprock bottom and salt top. A three-dimensional finite element model, which allows each cavern to be configured individually, was constructed to investigate horizontal and vertical displacements in each well as it crosses the various interbeds. The model contains interfaces between each lithology and a shear zone (fault) to examine the interbed behavior in a realistic manner. This analysis results indicate that the casings of Caverns 105 and 109 failed, respectively, from shear stress that exceeded the casing shear strength due to the horizontal movement of the salt top relative to the caprock and tensile stress due to the downward movement of the salt top from the caprock. The wellbores of Caverns 114 and 104, located at the far end of the field and near the fault, respectively, are predicted to fail by shear stress in the near future. The wellbores of inmost Caverns 107 and 108 are predicted to fail by tensile stress in the near future. The salt top subsides because the volumes of caverns in the salt dome decrease with time due to salt creep closure, while the caprock does not subside at the same rate as the salt top because the caprock is thick and stiff. This discrepancy yields deformation of the well.
机译:在大希尔战略石油储备站点的洞穴105和109的井眼中发现了漏油现象。根据现场观察,套管层底部和盐层顶部之间的夹层深度发生了两次套管破坏事件。构造了一个三维有限元模型,该模型允许每个洞穴分别进行配置,以研究每个井穿越不同夹层时的水平和垂直位移。该模型包含每个岩性和剪切带(断层)之间的接口,以实际方式检查夹层行为。该分析结果表明,洞穴105和109的套管分别由于盐顶相对于盖层的水平运动所引起的剪切应力超过了套管的剪切强度而失效,以及盐顶的向下运动所导致的拉伸应力分别导致了套管的破坏从顶极。预计分别位于油田远端和断层附近的洞穴114和104的井眼将在不久的将来因切应力而破裂。预计在不久的将来,最大洞穴107和108的井眼会因拉应力而失效。由于盐蠕变封闭,盐顶中的洞穴体积随时间减少而使盐顶消退,而盖层厚且坚硬,因此盖层的沉降速率与盐顶不一样。这种差异导致井的变形。

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