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Failure analysis of the repair procedure of an ore compactor roll

机译:压实机辊修复程序的失败分析

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摘要

This paper deals with the failure analysis of a potassium ore compactor roll that experi enced short term fracture in service after a repair procedure. The journal bearing of the shaft experienced wear after a long period in use. Afterwards, a surface deposition was per formed in order to retrieve the roll functionality, but it culminated in the formation of radial cracks beginning just near the shaft curvature radius. This portion of the roll was then removed and replaced with a new shaft interference-fitted and welded into the roll. Moreover, after this new repair procedure, the roll experienced a short term fracture. Fail ure analyses were performed by liquid penetrant, fracture analysis, hardness testing and metallographic analysis. Numerical simulations were also carried out considering the last repair features. Fatigue failure nucleated near a singularity at the shaft curvature radius. This singularity was originated from the interference fit and welding procedures.
机译:本文对钾矿石压实机辊在维修过程中在服役中经历了短期断裂的失效分析进行了分析。长期使用后,轴的轴颈轴承磨损。此后,为了恢复轧辊的功能性而进行了表面沉积,但最终形成了刚好在轴曲率半径附近开始的径向裂纹。然后取下这部分辊,并用过盈配合的新轴替换并焊接到辊中。而且,在这种新的修复程序之后,轧辊经历了短期断裂。通过液体渗透剂,断裂分析,硬度测试和金相分析进行失效分析。考虑到最后的维修功能,还进行了数值模拟。疲劳失效在轴曲率半径处接近奇点形核。这种奇异性源于过盈配合和焊接程序。

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