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Failure analysis of a welded outlet manifold pipe in a primary steam reformer by improper selection of materials

机译:一次蒸汽重整器中焊接出口歧管的材料选择错误分析

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摘要

A welded manifold pipe in a primary steam reformer used to transport hydrogen gas at about 873 deg C developed leakage in the weld fusion zone after about 22,000 h of operation. Detailed microstructural characterization using various electron-optical techniques and mechanical property evaluation were employed to determine the cause of failure. Selection of pipe material and filler metal with relatively high Si contents in the presence of Nb was found to be the cause of failure. It is shown that this combination had promotedintergranular precipitation of the embrittling Ni_3Nb_2Si laves phase in the weld fusion zone leading to loss of rupture ductility and associated cracking.
机译:在运行约22,000小时后,一次蒸汽重整器中用于在约873℃下输送氢气的焊接歧管在焊接熔合区产生泄漏。使用各种电子光学技术和机械性能评估进行详细的微结构表征,以确定故障原因。发现在Nb存在下选择具有较高Si含量的管道材料和填充金属是失败的原因。结果表明,这种结合促进了焊缝熔合区脆性Ni_3Nb_2Si Laves相的晶间析出,导致断裂延展性的丧失和相关的开裂。

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