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Column bioleaching characteristic of copper and iron from Zijinshan sulfide ores by acid mine drainage

机译:酸性矿山排水对紫金山硫化矿中铜和铁的柱浸出特性

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In Zijinshan, a commercial copper bio-heap leaching plant has been operating successfully since 2006. The plant used raffinate as irrigation solution and operated at low pH and high iron concentration from 2006 to 2010. However, high concentration of soluble iron led to crud formation and low current efficiency in subsequent solvent extraction and electro-winning (SX-EW) steps. It is important to reduce iron dissolution in bioleaching and address this low current efficiency issue. About 1500 m(3)/h acid mine drainage (AMD) accumulated in collection pool in the Zijinshan copper mine. Not only does it cause the loss of copper, but also result in potentially secondary pollution. This paper proposes an option to use AMD as leaching solution for the recovery of copper. Column bioleaching experiments were performed with low-grade secondary copper sulfide ore from Zijinshan. To simulate leaching, several variables such as irrigation solution, leachate treatment.(with or without recirculation), irrigation duration, temperature and pH were considered for the evaluation of the copper recovery and iron extraction. Results showed that 6-8 h/d irrigation was needed to ensure the wetting of the ore surface, to keep sufficiently high temperature and aeration inside the column. Under optimal pH condition of 1.6-1.8, with recirculation of AMD, copper leaching reached 90%, however iron leaching was only 20% both after 240 days, respectively. About 78-86% of copper extraction was observed in the first 100 days and then slight increase of about 4-12% towards the end, whereas iron extraction continued with an upward trend after 100 days. The results showed that AMD could be utilized for selective and efficient copper recovery in Zijinshan copper mine. (C) 2016 Elsevier B.V. All rights reserved.
机译:自2006年以来,紫金山市一家商业化的铜生物堆浸工厂已成功运行。该工厂从2006年至2010年使用萃余液作为灌溉溶液,并在低pH和高铁浓度下运行。但是,高浓度的可溶性铁导致了结块的形成。以及随后的溶剂萃取和电解沉积(SX-EW)步骤中电流效率低。重要的是减少生物浸出过程中铁的溶解并解决低电流效率问题。紫金山铜矿的收集池中累积了约1500 m(3)/ h的酸性矿井排水(AMD)。它不仅会导致铜的流失,还会导致潜在的二次污染。本文提出了一种选择将AMD用作铜回收的浸出解决方案。紫金山低品位次生硫化铜矿进行了柱生物浸出实验。为了模拟浸出,考虑了一些变量,例如灌溉溶液,渗滤液处理(有或没有再循环),灌溉持续时间,温度和pH值,以评估铜的回收率和铁的萃取率。结果表明,需要进行6-8 h / d的灌溉以确保矿石表面润湿,以保持足够的高温和柱内通气。在1.6-1.8的最佳pH条件下,随着AMD的再循环,铜浸出率分别达到90%,而铁浸出率在240天后均仅为20%。在开始的100天中观察到约78-86%的铜提取,然后到末期略有增加约4-12%,而在100天后铁提取继续以上升趋势。结果表明,AMD可用于紫金山铜矿的选择性高效铜回收。 (C)2016 Elsevier B.V.保留所有权利。

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