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An experimental study on the fault diagnosis of wind turbines through a condition monitoring system

机译:通过状态监测系统对风力涡轮机故障诊断的实验研究

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To detect wind turbine faults at an early stage, an investigation into a practical maintenance and repair approach was carried out on Jeju Island, South Korea. A condition monitoring system was installed in each wind turbine nacelle to detect the vibration signals from the gearbox and the generator. The vibration signals were measured by strain gauges on the gearbox and the generator for a period of approximately one to two years. A time domain analysis to detect the components' faults was performed, and a frequency domain analysis was conducted to find the location of the faults that occurred. Using the criteria of acceptance level for the root mean square suggested in Verein Deutscher Ingenieure standard 3834, it was determined whether or not the gearbox and the generator were operated normally. After a fault was detected by root mean square analysis, the fast fourier transform spectrum was analyzed and then compared with that suggested by the International Organization for Standardization standard 10816-21 and 13373-1. Repair work was then conducted on the defective parts of the components. The root mean square and the acceleration value of the normal, the warning and the abnormal conditions were compared with one another. As a result, cavitation might occur in the gear oil pump attached to the gearbox due to the high acceleration values observed for frequencies ranging from 5000 Hz to 11000 Hz. Additionally, the generator bearing at the non drive end was found to be broken because the defect frequency of the bearing was 88 Hz, which was derived from envelope spectrum analysis. The root mean square and the acceleration values for the gearbox and the generator decreased to values indicating normal operating conditions after the damage repair. The annual energy production increased by 1.8 % after the generator bearing repair.
机译:为了在早期阶段检测风力涡轮机故障,对韩国济州岛进行了对实际维护和维修方法的调查。每个风力涡轮机Nacelle安装了一个状态监测系统,以检测来自齿轮箱和发电机的振动信号。振动信号通过齿轮箱上的应变计和发电机测量大约一至两年的时间。执行检测组件故障的时域分析,并进行频域分析以查找发生故障的位置。利用在受体敏锡互联标准3834中建议的根均线的接受水平标准,确定齿轮箱和发电机是否正常运行。通过均方根分析检测到故障后,分析了快速傅里叶变换谱,然后与国际标准化标准10816-21和13373-1建议的建议进行比较。然后在组件的缺陷部件上进行维修工作。彼此比较了正常,警告和异常条件的根均线和加速度。结果,由于对于从500​​0Hz至11000Hz的频率观察到的高加速度值,在附接到齿轮箱的齿轮油泵中可能发生空化。另外,发现在非驱动端处的发电机轴承被破坏,因为轴承的缺陷频率为88Hz,其来自包络谱分析。齿条平方和变速箱的加速度和发电机减少到损坏修复后的正常操作条件的值。发电机轴承修复后,年度能源产量增加1.8%。

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