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Failure Analysis of API 5L (Grade B) Oil Field Separator Flowline Pipe

机译:API 5L(B级)油田分离器流动线管的故障分析

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摘要

This paper presents the root cause failure analysis of an API 5L (Grade B) pipe that failed while in full well stream service in the oil and gas industry. The operating temperature ranged from 120 to 190?°F and was exposed to hydrogen sulfide (H~(2)S) concentrations of 350–1000 ppm. Visual inspection, hardness test, metallography, Fourier transform infrared spectrophotometry, scanning electron microscopy, and energy-dispersive X-ray spectroscopy were carried out to investigate the pipe failure. This study revealed that an extremely localized pitting corrosion due to chloride attack was the main mode of the failure.
机译:本文介绍了在石油和天然气行业全井流服务中失败的API 5L(B级)管道的根本原因分析。 工作温度范围为120至190°F,并暴露于硫化氢(H〜(2)S)浓度为350-1000ppm。 进行目视检查,硬度测试,金相,傅里叶变换红外分光光度法,扫描电子显微镜和能量分散X射线光谱,以研究管道故障。 本研究表明,由于氯化物侵蚀引起的极其局部的点蚀腐蚀是故障的主要模式。

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