Ab'/> Solvent extraction separation of molybdenum as thio-molybdate complex from alkaline tungsten leach liquor of spent HDS catalyst – A pilot study
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Solvent extraction separation of molybdenum as thio-molybdate complex from alkaline tungsten leach liquor of spent HDS catalyst – A pilot study

机译:溶剂萃取分离钼作为碱性钨液中的硫代钼酸盐络合物,HDS催化剂 - 试验研究

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AbstractSpent nickel-tungsten catalyst generated from hydrotreating petroleum industry always contains molybdenum about 0.1–2% as an impurity. Separation of Mo from spent Ni-W catalyst leach solutions is a critical step to produce high pure tungsten products like ammonium paratungstate (APT) and tungsten trioxide (WO3) for catalyst and tools applications. Though Mo and W have chemically similar properties but it is possible to exploit separation of Mo from W by modifying the aqueous phase species. In the present paper, alkaline leach liquor with a composition of 0.72g/L Mo and 18g/L W was taken. Selective separation of Mo as its thiocomplex from W was examined by Aliquat 336, a quaternary ammonium compound. Experimental parameters such as extraction pH, concentration of extractant and metal for extraction and selection of reagent and concentration for stripping were optimized to obtain maximum separation of Mo. Variation of extractant concentration indicated extracted Mo species as (R3CH3N)2MoS4. The McCabe-Thiele plots indicated that 2 and 3-counter-current stages are necessary at O:A ratio of 1:1 and 3:1 for quantitative extraction and stripping of molybdenum, respectively. A pilot run for 330h was operated with 3-stages of extraction, 1-stage of scrubbing, 3-stages of stripping and one stage of washing based on the equilibrium data to verify the performance of Mo separation from W from commercial point of view.Highlights?Condition optimized for complete thionisation of MoO42?to MoS42?.?3% Aliquat 336+3% Exxal D10 was used as extractant.?McCabe-Thiele plot showed 2 stages of extraction at unity O:A ratio.?The extracted species was determined to be (R3CH3N)2MoS4.]]>
机译:<![cdata [ 抽象 从加氢处理石油工业中产生的镍钨催化剂总是含有约0.1-2%作为杂质的钼。来自镍氢铝催化剂浸出溶液的MO分离是生产高纯钨产物的副钨酸盐(APT)和三氧化钨(WO 3 )的关键步骤用于催化剂和工具应用。虽然Mo和W具有化学相似的性质,但是可以通过改变水相物质来利用Mo的分离。在本文中,采用具有0.72g / L Mo和18g / L W的组成的碱性浸出液。通过AliquataT 336,季铵化合物检查从W.Siqualat 336,通过AliquataT 336检查Mo作为其硫代络合物的选择性分离。优化诸如提取pH,萃取剂浓度和金属萃取和选择试剂和剥离浓度的实验参数,得到MO的最大分离。提取物浓度的变异表明提取的MO物种(R 3 CH 3 N) 2 MOS 4 。 McCabe-Thiele图表明,用于定量萃取和汽提的钼的比例为1:1和3:1的比例。使用330H的试验运行330H,用3级的萃取,擦洗,3级的3阶段,基于平衡数据的一个洗涤阶段,以验证来自商业角度的Mo分离的Mo分离的性能。 亮点 条件优化以完成完全决定moo 4 2?到mos 4 2? 3%Aliquat 336 + 3%exxa L D10用作萃取剂。 mccabe-thiele图显示Unity O:a比率的2个提取阶段。 所提取的物种被确定为(r 3 / CE:INF> CH 3 N) 2 MOS 4> 4 ]]>

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