...
首页> 外文期刊>World Pumps >Oil & gas: Full refurbishment for island refinery
【24h】

Oil & gas: Full refurbishment for island refinery

机译:石油和天然气:岛炼油厂完全翻新

获取原文
获取原文并翻译 | 示例

摘要

After a refinery closed down its 50-year old plant, most of the rotating equipment suffered damage from exposure to the tropical climate. To restart the plant, the new owners called upon Hydro, Inc., to reverse engineer, rebuild and perform testing on their critical jet pump. The process of reopening the plant had uncovered more than 500 pumps that needed considerable refurbishment and repair. The most important of these was a critical jet pump used for hydraulic decoking. It was badly damaged and sent to the original equipment manufacturer (OEM) for inspection. The OEM recommended that the refinery replace most of the pump parts, as well as a costly repair that would require 35 weeks to rebuild. Viable alternative Instead, the refinery sent the pump to global aftermarket pump service provider, Hydro, Inc. in Chicago, where it was refurbished for just over half the cost of the OEM proposal. The time involved was also significantly improved to just eight weeks by using a non-destructive evaluation and rebuild process at a 46,000 ft~2 facility where Hydro develops and implements engineering modifications for improving the performance of critical pumps and then verifies that performance in their Hydraulic Institute certified test lab. Significant reopening. The original refinery opened in the mid 1960s. In the early 1970s, it was re-rated at 650,000 barrels per day. It had been one of the largest refineries in the western hemisphere, so the impact of reopening the plant would be significant. In this case, Hydro was tasked to work with the critical high-energy pump to prepare for its reopening. The new owners began the process two years ago and it is expected that the plant will be open for operation in the first quarter of 2020. Once restarted, the plant will be able to process up to 210,000 barrels per day of oil, a fraction of the 1,500-acre (607-hectare) plant's peak capacity in the 1970s of 650,000 bpd.
机译:在炼油厂关闭50岁的植物后,大多数旋转设备因暴露于热带气候而受到伤害。要重新启动工厂,新所有者呼吁Hydro,Inc。,逆向工程师,重建并在其临界喷射泵上进行测试。重新打开植物的过程已经未覆盖500多个泵,需要相当多的翻新和修复。其中最重要的是用于液压毁灭的关键喷射泵。它被严重损坏并送到原始设备制造商(OEM)进行检查。 OEM建议炼油厂替换大部分泵部件,以及需要35周的昂贵的修复才能重建。可行的替代品,炼油厂将泵发送到全球售后市场泵服务提供商,Hydro,Inc。在芝加哥,它被翻新,仅为OEM提议的成本超过一半。通过使用非破坏性评估和重建过程,在46,000 FT〜2设施下,所涉及的时间也显着改善了仅仅八周的时间。研究所认证测试实验室。重新开放。原始炼油厂于20世纪60年代中期开业。在20世纪70年代初,它每天重新评估650,000桶。它是西半球最大的炼油厂之一,因此重新开放工厂的影响将是显着的。在这种情况下,Hydro任务是使用临界高能量泵,为其重新开放做好准备。这位新的主人两年前开始了这个过程,预计该工厂将在2020年的第一季度开放运营。一旦重新开始,该工厂将能够每天生产高达210,000桶油,这是一小部分20世纪70年代的1,500英亩(607公顷)的植物峰值容量为650,000 bpd。

著录项

  • 来源
    《World Pumps 》 |2020年第632期| 共3页
  • 作者

  • 作者单位
  • 收录信息
  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类 泵 ;
  • 关键词

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号