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首页> 外文期刊>Journal of Failure Analysis and Prevention >Fatigue Failure of LP Compressor Blade in an Aero Gas Turbine Engine
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Fatigue Failure of LP Compressor Blade in an Aero Gas Turbine Engine

机译:航空燃气轮机发动机低压压缩机叶片的疲劳失效

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摘要

Failure of low-pressure compressor rotor blade in an aero gas turbine engine is analyzed to determine its root cause. Forensic and metallurgical investigations are carried out on the blade failed. The failure of the first stage rotor blade is found to be the first in the chain of events that led to the engine failure. The mode of failure in the blade is found to be fatigue and has originated from the mounting lug fillet region due to high stress concentrations. The failure has caused extensive damages in low-pressure compressor module and also in downstream modules as a secondary effect. Remedial measures are also suggested to prevent such failures.
机译:分析了航空涡轮发动机中低压压缩机转子叶片的故障,以确定其根本原因。对失败的刀片进行法医和冶金研究。发现第一级转子叶片的故障是导致发动机故障的一系列事件中的第一个。发现叶片中的故障模式是疲劳的,并且由于高应力集中而源自安装凸耳圆角区域。该故障已对低压压缩机模块和下游模块造成了广泛的损害,这是次要作用。还建议采取补救措施以防止此类故障。

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