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首页> 外文期刊>Transactions of the Indian Ceramic Society >Modified Design and Lining of Tunnel Kiln for Indian Crockery Industry to Improve Furnace Efficiency
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Modified Design and Lining of Tunnel Kiln for Indian Crockery Industry to Improve Furnace Efficiency

机译:印度陶器业隧道窑的改进设计和衬里,以提高炉子效率

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摘要

In India, a large number of ceramicware manufacturers are actively engaged in small / medium sectors with production capacities varying from 500 to 1500 tons per annum. These units are largely located in northern and western India. Average oil consumption of these industries are in the range of 170-250 L.ton~(-1) of product. Initial study conducted in some of these industries reveals that there is large temperature gradient across the height of the kiln and excess oxygen in all zones. Kiln shell temperature also is very high in all of these kilns. Also, the insulation system of kiln car lining is very erratic and often leads to failure and consequent loss of production. Based on the findings, it was decided to incorporate changes in design concepts in some of the kilns and optimize temperature, pressure and combustion regimes of the furnaces. Implementation of all the modifications in two kilns has resulted in increase in productivity by 30-35% and reduction in specific fuel consumption by 15-20%.
机译:在印度,许多陶瓷制品制造商正积极参与中/小型行业,其年生产能力从500吨到1500吨不等。这些单位主要位于印度北部和西部。这些行业的平均油耗在170-250 L.ton〜(-1)产品范围内。在其中一些行业中进行的初步研究表明,在整个窑炉高度上存在较大的温度梯度,并且在所有区域中都有过量的氧气。在所有这些窑中,窑壳温度也很高。而且,窑车衬里的隔热系统非常不稳定,经常导致故障并因此导致生产损失。根据调查结果,决定在某些窑炉中纳入设计概念的变化,并优化炉子的​​温度,压力和燃烧方式。在两个窑炉中实施所有修改后,生产率提高了30-35%,比燃料消耗降低了15-20%。

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