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Effective method for adjusting the uplifting of shield machine tunneling in upper-soft lower-hard strata

机译:用于调整上软低硬层屏蔽机隧穿屏蔽机隧道的有效方法

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摘要

The control and treatment of excessive uplifting of a shield machine during tunneling in the upper-soft lowerhard strata is challenging. This is because buoyancy of the shield machine is induced by the gap between the shield machine and the ground, and the upper ground has less resistance than the lower ground in the upper-soft lower-hard composite strata. In this paper, a new method for adjusting the excessive uplifting of a shield tunnel machine is proposed. This method utilizes a special drill beneath the shield machine's cutter head that operates on the middle shield machine position and can result in subsidence of the ground under the heavy weight of the shield machine. Based on this new technique, a case study of the excessive uplifting of a shield tunnel machine in the line No. 3 of China's Nanning Metro is presented. The shield tunnel machine's maximum uplifting amount of 118 mm was successfully corrected, and the treatment processes had no influence on the surrounding environment. The correction method for the excessive uplifting of shield machines proposed in this study can provide a reference for future projects with similar conditions.
机译:在隧道隧道中隧道屏蔽机上过度振奋的控制和处理是具有挑战性的。这是因为屏蔽机的浮力由屏蔽机和地之间的间隙引起,并且上地具有比上软低硬化组合层中的下地的电阻较小。在本文中,提出了一种调整屏蔽隧道机的过度振奋的新方法。该方法采用屏蔽机的刀具头下方的特殊钻头,在中间屏蔽机位置上运行,可以在屏蔽机的重量下导致地面的沉降。基于这种新技术,提出了对中国南宁地铁3号线过度振奋的屏蔽隧道机的过度振奋的案例研究。屏蔽隧道机的最大升高量为118毫米,并对周围环境没有影响。本研究提出的屏蔽机的过度振衡的校正方法可以为未来项目提供相似条件的投资提供参考。

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