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UPGRADE OF CONTROL AND PROTECTION SYSTEM OF THE IGNALINA NUCLEAR POWER PLANT UNITS 1 AND 2

机译:IGNALINA核电站1和2的控制和保护系统的升级

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The Ignalina nuclear power plant (NPP) Units 1 and 2 are Soviet-designed, RBMK (Reaktor Bolshoi Moschnosti Kipyashchiy), channelized, large power-type reactors. The original-design electrical capacity for each unit was 1500 MW. Unit 1 began operating in 1983, and Unit 2 was started up in 1987. In 1994, the government of Lithuania agreed to accept grant support for the Ignalina NPP Safety Improvement Program with funding supplied by the Nuclear Safety Account of the European Bank for Reconstruction and Development (EBRD). As conditions for receiving this funding, the Ignalina NPP agreed to prepare a comprehensive safety analysis report that would undergo independent peer review after it was issued. The EBRD Safety Panel oversaw preparation and review of the report. In 1996, the safety analysis report for Unit 1 was completed and delivered to the EBRD. Part of the analyses covered anticipated transients without scram (ATWS). The analysis showed that some ATWS scenarios could lead to unacceptable consequences in <1 min. The EBRD Safety Panel recommended to the government of Lithuania that the Ignalina NPP develop and implement a program of compensatory measures for the control and protection system before the unit would be allowed to return to operation following its 1998 maintenance outage. A compensatory control and protection system that would mitigate the unacceptable consequences was designed, procured, manufactured, tested, and installed. The project was funded by U.S. Department of Energy.
机译:伊格纳利纳核电站(NPP)的1号和2号机组是苏联设计的RBMK(Reaktor Bolshoi Moschnosti Kipyashchiy)通道化大型功率反应堆。每个单元的原始设计电容量为1500 MW。 1号机组于1983年开始运行,2号机组于1987年开始运行。1994年,立陶宛政府同意接受由欧洲复兴开发银行和欧洲复兴开发银行核安全帐户提供的资金支持Ignalina NPP安全改进计划。发展(EBRD)。作为获得这笔资金的条件,Ignalina NPP同意准备一份全面的安全分析报告,该报告在发布后将接受独立的同行审查。欧洲复兴开发银行安全小组监督了报告的准备和审查。 1996年,第1单元的安全分析报告已经完成并提交给欧洲复兴开发银行。部分分析涵盖了预期的无扰动瞬变(ATWS)。分析表明,某些ATWS场景可能在不到1分钟的时间内导致无法接受的后果。欧洲复兴开发银行安全小组向立陶宛政府建议,伊格纳利纳核电厂应制定并实施一项控制和保护系统补偿措施计划,然后该机组才能在1998年维护中断后恢复运行。设计,采购,制造,测试和安装了可减轻不可接受后果的补偿性控制和保护系统。该项目由美国能源部资助。

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