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Using modified fly ash for mercury emissions control for coal-fired power plant applications in China

机译:在中国燃煤电厂应用改性粉煤灰控制汞排放

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摘要

More than 50% of the mercury emissions in China come from coal-fired power plants. Coal-fired power plants also consume more than 50% of the coal used in China, and this proportion is expected to increase according to Chinese energy planning agencies, despite recent actions aiming at more stringent environmental constrains. This study reports mercury emissions measurements of several power plants in China. The results show that the mercury concentration in the flue gas has variability between 0.19 and 11.30 mu g/Nm(3). At the same time, the co-benefit of mercury removal by the existing pollutant control devices at those plants was highly variable, ranging from 17.8% to 96.7%. This motivated research on developing and testing a modified fly ash sorbent that would be competitive due to its low cost, in relative abundance, and adequate for convenient injection at a power plant. Full-scale injection and adsorption experiments were performed at a 300 MW plant. It was found that the use of a modified fly ash provide an additional mercury emissions reduction, in addition to the inherent natural mercury capture by the host unit of 30% due to additional fly ash adsorption. Implementation of this additional control option would help achieve combined mercury removal efficiencies in the 75-90% range. (C) 2016 Elsevier Ltd. All rights reserved.
机译:在中国,超过50%的汞排放来自燃煤电厂。燃煤电厂也消耗了中国50%以上的煤炭,据中国能源规划机构称,尽管最近采取了更加严格的环境约束措施,但这一比例仍有望增加。这项研究报告了中国几座发电厂的汞排放量测量结果。结果表明,烟气中的汞浓度在0.19和11.30μg / Nm(3)之间变化。同时,那些工厂现有的污染物控制装置除汞的共同收益变化很大,范围从17.8%到96.7%。这项有动机的研究致力于开发和测试改性粉煤灰吸附剂,该吸附剂因其成本低,相对丰富而具有竞争力,并且足以在电厂中方便地注入。在300 MW的工厂进行了大规模的注入和吸附实验。已经发现,使用改性粉煤灰可进一步减少汞排放,此外,由于额外的粉煤灰吸附,主体单元固有的天然汞捕获量也可减少30%。实施此附加控制选项将有助于实现75-90%范围内的综合除汞效率。 (C)2016 Elsevier Ltd.保留所有权利。

著录项

  • 来源
    《Fuel》 |2016年第1期|1230-1237|共8页
  • 作者单位

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China|Western Kentucky Univ, Inst Combust Sci & Environm Technol, Bowling Green, KY 42101 USA;

    Lehigh Univ, Energy Res Ctr, 117 ATLSS Dr, Bethlehem, PA 18015 USA;

    North China Elect Power Univ, Minist Educ, Key Lab Condit Monitoring & Control Power Plant E, Beijing 102206, Peoples R China|Western Kentucky Univ, Inst Combust Sci & Environm Technol, Bowling Green, KY 42101 USA;

  • 收录信息 美国《科学引文索引》(SCI);美国《工程索引》(EI);
  • 原文格式 PDF
  • 正文语种 eng
  • 中图分类
  • 关键词

    Mercury emissions control; Modified fly ash; Power plants in China;

    机译:汞排放控制;改性粉煤灰;中国发电厂;

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