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Analysis of the bedding landslide due to the presence of the weak intercalated layer in the limestone

机译:石灰岩中存在弱插层引起的顺层滑坡分析

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Analysis and research results show that the sliding plane of Jiudingshan landslide is along the weak intercalated layer (clay-filled) in the limestone and the sliding block is separated by the tension crack on the slope crest. The earlier study results show that for the rough, ups and downs structural plane, when i is greater than 2.0, the shear strength of the structural surface is intensely close to the strength of the filling. By the earlier theory, this failure must be through the clay filling. In this study, the failure is back-analyzed and the shear strength of the infilling is tested by the laboratory direct shear tests for which samples were retrieved in the field. The failure cannot be explained by the laboratory results of shear strength parameters. To simulate the field conditions, the real strength parameters of sliding surface are measured by the in situ shear tests for the weak intercalated layer. By the in situ tests, it is shown that the failure initiates along the contacts between the clay infilling and the limestone boundaries, but not through the clay itself. Though the contact surface is the interface of the clay-limestone, the cohesion is not 0 and it is not negligible too.
机译:分析和研究结果表明,九顶山滑坡的滑动面沿石灰岩中的薄弱夹层(填土),并且滑坡被斜坡上的张力裂缝所分隔。较早的研究结果表明,对于粗糙的,起伏的结构平面,当i大于2.0时,结构表面的剪切强度与填充物的强度非常接近。根据较早的理论,这种失败必定是通过粘土填充。在这项研究中,对破坏进行了反分析,并通过实验室直接剪切测试对填充物的剪切强度进行了测试,在现场直接提取了样品。不能通过剪切强度参数的实验室结果来解释失效。为了模拟现场条件,通过对弱插层的原位剪切试验测量了滑动面的真实强度参数。通过原位测试表明,破坏是沿着黏土填充物和石灰岩边界之间的接触而不是通过黏土本身引发的。尽管接触表面是粘土-石灰石的界面,但是内聚力不是0,也不能忽略。

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