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A new method of foam drainage technology in loading gas well

机译:气井加载中泡沫排水技术的新方法

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Foam drainage technology has been widely used to remove the liquid out of pipe in loading gas wells and keep the well normally producing. Still, it has some limitation in application, especially for the wells in low temperature and remote areas, which are commonly protected by the attemperator and alcohol injection in the wellhead. Faced with these limitation, we propose a new way, which owns the following advantages: 1) it keeps the original devices, 2) it solves the problem of hardly dissolvability of original injecting alcohol and newly injecting defoamer, and makes use of the alcohol injecting equipment as co-defoaming process, 3) the ability of anti-freezing and defoaming is maintained, which is the base of application, 4) the main costs of the new method are the expense of necessary chemical agents, making the method quite economical. Further, the new method was applied into the severely loading gas well, it turned out that the effect of anti-freezing and defoaming was obvious and the well had been brought back into live. Besides, the frequency of shut-in was reduced by a large extent. Our study suggests that the new method could be popularized in remote gas wells in low temperature environment if suitable foamer, defoamer and emulsifier could be provided.
机译:泡沫排水技术已被广泛用于从装载气井中的管道中清除液体,并保持气井正常生产。但是,它在应用中仍然有一些局限性,特别是对于低温和偏远地区的井,这些井通常受到井口的调温剂和酒精注入的保护。面对这些局限性,我们提出了一种新方法,它具有以下优点:1)保留了原有的装置; 2)解决了原有注入的酒精和新注入的消泡剂难以溶解的问题,并利用注入的酒精作为共消泡工艺的设备,3)保持了防冻和消泡的能力,这是其应用的基础。4)新方法的主要成本是必需化学试剂的费用,使该方法非常经济。进而,将该新方法应用于重载气井中,结果表明,防冻消泡效果明显,该井已恢复生产。此外,关闭的频率大大降低了。我们的研究表明,如果能够提供合适的发泡剂,消泡剂和乳化剂,该新方法可以在低温环境下的偏远气井中推广。

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