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Case study of deformation geotextile reinforced earth wall using mudstone

机译:泥岩变形土工布加筋土墙实例研究

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In recent years, cases where reinforced earth walls were adopted in the construction of expressways are increasing. On the other hand, damages and deformations of these walls have been reported. In this paper we will take up deformations that had developed in a geotextile reinforced earth wall using mudstone. Deformations to this earth wall developed one year after construction, and consequently, the wall was rebuilt. Various tests were carried out at the time of the reconstruction to study the case and find the cause of the deformation. Testing and research showed low relative weaknesses of the wall, such as high water content at the upper wall and around the front face of the upper wall, and low shear wave velocity. From the results, we have concluded that the deformation was caused by water penetrating from the road surface and drainage facilities of the reinforced earth wall backfill. In the testing, we were able to confirm the validity of the surface wave exploration and that the strength of the geotextile reinforcements used in the deformed area had lowered.
机译:近年来,在高速公路建设中采用加筋土墙的情况越来越多。另一方面,已经报道了这些壁的损坏和变形。在本文中,我们将处理在使用泥岩的土工织物加筋土墙中产生的变形。土墙的变形是在施工一年后发展的,因此,该墙被重建。重建时进行了各种测试,以研究案例并找出变形的原因。测试和研究表明,该壁的相对弱度较低,例如,上壁和上壁正面周围的含水量较高,剪切波速较低。从结果可以得出结论,变形是由于水从加筋土墙回填的路面和排水设施渗入而引起的。在测试中,我们能够确认表面波勘探的有效性,并且在变形区域使用的土工布增强材料的强度已经降低。

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