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Development and Optimization of the Die-Sinking EDM-Technology for Machining the Nickel-based Alloy MAR-M247 for Turbine Components

机译:涡轮零件用镍基合金MAR-M247的冲裁电火花加工技术的开发和优化。

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In this paper, the results regarding the optimization of the die-sinking EDM-technology for the fabrication of turbine components are presented. The main objective of this work was the reduction of machining time while producing cavities with a depth of 11mm in the alloy MAR-M247, with respect to the requirements for surface roughness and sub-surface damage. The study was conducted using graphite electrodes of three different dimensions, totalizing 12 electrodes and a total electrode area of 89.50 mm2. The machine tool GENIUS 1000 THE CUBE was used in the experiments and IonoPlus IME-MH was used as dielectric fluid. The Design of Experiments Methods (DoE) were applied in the planning and execution of all experiments. Firstly, experiments were conducted to estimate the maximal discharge current that can be applied for fulfilling the quality criteria regarding both surface roughness and thickness of affected sub-surface, since discharge current is known as the main influencing process parameter affecting both factors. In the second stage, the process was optimized by varying following electrical parameters of the machine tool: discharge current (ie), discharge duration (ti), pause duration (t0), ignition voltage (V) and duty factor (τ). Finally, both process parameters as well as machine tool's control parameters were adjusted to achieve optimized results regarding the total machining time and electrode wear with respect to the surface requirements of produced parts. A total machining time reduction of more than 50% in comparison to the technology currently employed by the industry was achieved. Requirements on both arithmetical surface roughness as well as affected sub-surface thickness could be fulfilled. This robust technology was developed for producing the cavities in MAR-M247 and all applied methods, studied parameters as well as the results regarding machining time, electrode wear and the quality of the achieved work piece are presented.
机译:在本文中,介绍了有关用于制造涡轮机部件的冲模电火花成形技术的优化结果。这项工作的主要目的是减少加工时间,同时根据表面粗糙度和亚表面损伤的要求,在MAR-M247合金中生产深度为11mm的型腔。该研究使用了三个不同尺寸的石墨电极,总共12个电极,总电极面积为89.50 mm2。实验中使用了机床GENIUS 1000 THE CUBE,而IonoPlus IME-MH被用作介电液。实验设计方法(DoE)用于所有实验的计划和执行。首先,进行实验以估计可用于满足有关表面粗糙度和受影响的子表面厚度的质量标准的最大放电电流,因为已知放电电流是影响两个因素的主要影响工艺参数。在第二阶段中,通过更改机床的以下电气参数来优化过程:放电电流(即),放电持续时间(ti),暂停持续时间(t0),点火电压(V)和占空比(τ)。最后,调整工艺参数以及机床的控制参数,以获得关于总加工时间和电极磨损(相对于所生产零件的表面要求)的优化结果。与行业目前采用的技术相比,总加工时间减少了50%以上。可以满足对算术表面粗糙度以及受影响的子表面厚度的要求。开发了用于在MAR-M247中生产型腔的强大技术,并采用了所有应用的方法,研究了参数以及有关加工时间,电极磨损和所获得工件质量的结果。

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