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Reliability Analysis of Super 13Cr Tubing in Ultra-Deep Gas Well

机译:超深气井中超13Cr油管的可靠性分析

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Abnormal oil casing pressure appeared in the process of test production of multiple Ultra-Deep Gas Wells in Tarim Basin. The super 13Cr oil pipe string was used to analyze the causes of pipe string failure in view of the oil casing channeling well during the test and blowout period. The construction process of the well was analyzed in detail. Combined with the review of the operation flow and the detection of fracture string material and fracture morphology, the causes of pipe string fracture were analyzed and calculated in detail. Through field investigation, analysis and calculation, it was found that the main cause of cracking of super 13Cr tubing in this well is the decrease of vibration natural frequency caused by excessive fluid velocity in pipe and too long span of pipe string. At the same time, the mixed failure of stress corrosion cracking and stress load interaction occurred in Cl~( − 1) environment and other corrosion environments.
机译:塔里木盆地多口超深天然气井试生产过程中出现了异常的套管压力。鉴于在测试和井喷期间油套管窜动良好,使用超级13Cr油管柱分析了管柱失效的原因。对该井的建设过程进行了详细分析。结合对作业流程的回顾,对裂缝管柱材料和裂缝形态的检测,对管柱破裂的原因进行了详细的分析和计算。通过现场调查,分析和计算,发现该井超13Cr油管开裂的主要原因是由于管内流体流速过大和管柱跨度过长所引起的振动固有频率降低。同时,在Cl〜(#8722; 1)环境和其他腐蚀环境中发生了应力腐蚀开裂和应力载荷相互作用的混合破坏。

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