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首页> 外文期刊>International Journal of Coal Science & Technology >Experimental research on overlying strata movement and fracture evolution in pillarless stress-relief mining
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Experimental research on overlying strata movement and fracture evolution in pillarless stress-relief mining

机译:无柱卸压采煤上覆岩运动与裂缝演化试验研究

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In multiple seams?mining, the seam with relatively low gas content (protective seam) is often extracted prior to mining its overlying and/or underlying seams of high gas content and low permeability to minimize the risk of high gas emission and outbursts of coal and gas. A key to success with this mining sequence is to gain a detailed understanding of the movement and fracture evolution of the overlying and underlying strata after the protective seam in extracted. In Zhuji mine, the No. 11-2 seam is extracted as a protective seam with the pillarless mining method by retaining goaf-side roadways prior to its overlying No. 13-1 seam. An investigation has been undertaken in the panel 1111(1) of Zhuji mine to physically simulate the movement and fracture evolution of the overlying strata after the No. 11-2 seam is extracted. In the physical simulation, the displacement, strain, and deformation and failure process of the model for simulation were acquired with various means such as grating displacement meter, strain gauges, and digital photography. The simulation result shows that: (1) Initial caving interval of the immediate roof was 21.6?m, the first weighting interval was 23.5–37.3?m with the average interval of 33.5?m, and the periodic weighting interval of the main roof was in a range of 8.2–20.55?m and averaged at 15.2?m. (2) The maximum height of the caving zone after the extraction of No. 11-2 seam was 8.0?m, which was 4 times of the seam mining height and the internal strata of the caving zone collapsed irregularly. The mining-induced fractures developed 8–30?m above the mined No. 11-2 seam, which was 7.525 times of the seam mining height, the fracture zone was about 65° upward from the seam open-off cut toward the goaf, the height of longitudinal joint growth was 4–20 times of the mining seam height, and the height of lateral joint growth was 20–25 times of the mining seam height. (3) The “arch-in-arch” mechanical structure of the internal goaf was bounded by an expansion angle of broken strata in the lateral direction of the retained goaf-side roadway. The spatial and temporal evolution regularities of overburden’s displacement field and stress field, dynamic development process and distribution of fracture field were analyzed. Based on the simulation results, it is recommended that several goaf drainage methods, i.e. gas drainage with buried pipes in goaf, surface goaf gas drainage, and cross-measure boreholes, should be implemented to ensure the safe mining of the panel 1111(1).
机译:在多煤层开采中,通常在开采高瓦斯含量和低渗透率的上覆层和/或下覆层煤层之前先抽出相对低瓦斯含量的煤层(保护性煤层),以最大程度地减少高瓦斯涌出和煤与瓦斯突出的风险。加油站。开采顺序成功的关键是要对开采保护层后的上覆岩层和下覆岩层的运动和裂缝演化有一个详细的了解。在诸暨矿区,通过在上覆13-1号煤层之前保留采空区侧巷道,采用无柱开采方法将11-2号煤层作为保护性层开采。在诸暨矿区面板1111(1)进行了调查,以物理模拟开采11-2号煤层后上覆地层的运动和裂缝演化。在物理仿真中,通过各种方法(例如光栅位移计,应变仪和数码摄影)获取用于仿真的模型的位移,应变以及变形和破坏过程。仿真结果表明:(1)紧邻顶板的初始崩落间隔为21.6?m,第一加权间隔为23.5-37.3?m,平均间隔为33.5?m,主顶棚的周期性加权间隔为范围为8.2–20.55?m,平均为15.2?m。 (2)11-2号煤层开采后的崩落带最大高度为8.0?m,是该煤层开采高度的4倍,崩落带内部地层不规则塌陷。开采引起的裂缝在所开采的11-2号煤层上方发展了8-30?m,是煤层开采高度的7.525倍,裂缝区域从煤层露头切向煤层向上约65°,纵向缝的生长高度是煤层高度的4–20倍,横向缝的生长高度是煤层高度的20–25倍。 (3)内部采空区的“拱形”机械结构以破裂的地层在保留的采空区侧巷道的横向上的扩展角为边界。分析了覆盖层位移场和应力场的时空演化规律,动态发育过程和裂缝场分布。根据模拟结果,建议采取多种采空区抽采方法,例如采空区中埋有埋管的瓦斯抽采,地面采空区瓦斯抽采和跨孔钻孔,以确保面板1111(1)的安全开采。 。

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