While in cruise flight, pilot noticed smoke coming out from under instrument panel. Pilot aborted flight but noticed landing gear extension much slower than normal. Aircraft was placed on jacks and gear retracted. Pump motor (p 98811281) could be heard grinding and working very slowly. Pump motor was too hot to be touched. Battery was disconnected, aborting retraction. New pump and motor were installed. Teaching plain vanilla unusual attitude recovery for more than 80 years hasn't been successful in keeping the loss of control accident rate under control. Moving to LOC avoidance and recovery training that emphasizes the why of LOC, the risk factors leading to it, avoiding it and realistic in-flight simulations and recovery is the logical next step. Besides, the training is a lot of fun.
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