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Case Report: Persistent urinary incontinence after a robot-assisted artificial urinary sphincter procedure: lessons learnt from two cases

机译:病例报告:机器人辅助人工尿道括约肌手术后持续性尿失禁:两个案例的经验教训

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摘要

This case report describes 2 cases of persistent urinary incontinence in the beginning of the learning curve of robot-assisted bladder neck implantation of an artificial urinary sphincter (RA-AUS) in men at risk for erosion due to neurological lesions. Among a series of 4 RA-AUS, 2 patients still experienced urinary incontinence after surgery. A complete urological workup was strictly normal and did not show any device malfunction. However, during an AUS revision in these two patients, exploration revealed that the cuff was not tight enough. This issue was resolved by placing smaller cuffs. After re-do surgery, one of the two patients no longer had urinary incontinence, while the second patient was lost to follow-up. Insufficient tightness of the cuff could be explained by an inability of the surgeon to feel the force while pulling the cuff around the urethra due to the absence of haptic sensation in robotic surgery.
机译:该病例报告描述了2例在男性因神经系统病变而有糜烂风险的机器人辅助膀胱括约肌(RA-AUS)人工膀胱括约肌的学习曲线开始时出现持续性尿失禁的病例。在一系列的4种RA-AUS中,有2名患者术后仍出现尿失禁。严格的泌尿科检查完全正常,没有显示任何设备故障。但是,在这两名患者的AUS翻修期间,研究发现,袖带不够紧。通过放置较小的袖口可以解决此问题。再次手术后,两名患者中的一名不再患有尿失禁,而另一名患者失去随访。由于机器人手术中没有触觉,外科医生无法在拉动袖带绕尿道时感觉不到力,因此可以解释袖带的紧缩程度不足。

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